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Conference asdg::cmp

Title:CMP
Notice:Welcome to the CMP notesfile
Moderator:FABSIX::B_TOWERLLE
Created:Tue Oct 31 1995
Last Modified:Fri Jun 06 1997
Last Successful Update:Fri Jun 06 1997
Number of topics:94
Total number of notes:6381

45.0. "CMP-SCRUB.A1 EE/PE PASSDOWNS " by SUBPAC::BJUBINVILLE (NFD Fire - Rescue) Fri Dec 08 1995 22:20

    
         THIS NOTE IS DEDICATED FOR THE EQUIPMENT PROCESS
         ENGINEERING PASSDOWNS FOR:
    
                                            CMP-SCRUB.A1
T.RTitleUserPersonal
Name
DateLines
45.52brush height problem; lift arm the culpritSUBPAC::LANDRYSun Nov 12 1995 19:1713
    There was a positional problem with the brush height today in the
    outside brush station.  When in the scrub position, the mechanical
    stop wasn't making contact with the top of the micrometer.  The
    arm thats attached to the bimba cylinder seemed to have loosen
    enough to cause this situation.
    
    Therefore, the micrometers were checked to assure that the proper
    settings still existed, which they did.  So, we physically adjusted the
    arm and re-tightened the the bolt.  Checked for brush contact with the
    wafer at the spin position.  Tested fine.
    
    						A Shift
    
45.53Robot FingersFABSIX::R_GEEMon Nov 13 1995 07:1619
	* The robot fingers wouldn't close properly.

	  Checked the robot and spin station spindle for any loose
	  hardware, everything looked good.

	  Adjusted the teflon spring between the robot arms to even the
	  distance between the fingers and the wafer.

	  Changed the off-set position for Rotation at Spin from 871 
	  to 879.

	  Changed the off-set position for Robot Fingers from 260
	  to 210.
	  
	  Re-adjusted the Fingers Closed flag.

	  Ran 50 verification wafers, everything looks good.

					B shift & Mitch
45.54DI attack!!!!SUBPAC::BJUBINVILLENFD Fire - RescueThu Nov 23 1995 06:3532
    
    
        The status of SCRUB.A1 is as listed.  DI water worked
     its way through the bearings, through the spindle shaft
     and the spindle tube.  The bearings and tube are rusted and
     are binding.  The DI water also got down to the motor which
     is why the machine went down in the first place.  The motor
     was stopping during the spin cycle.  The motor is in stock
     and should be replaced.  Whom ever calls for the rush order,
     see if they can assemble the outer spindle assembly.  We
     have limited access to any presses and would save alot of time.
     I could put it back together but if OPS wants it when the parts
     come in, it might be just as easy to get Ron in.

Parts needed to be ordered...

OnTrak ID #

            (1) 13-0082-029   spindle shaft
            (1) 13-0082-024   spindle tube
            (1) 13-8082-073   splash gaurd, 200mm
            (1) 90-0033-019   flat washer, 7/8 OD  
            (2) 201-036       ball bearing, .50 bore, 1.12
            (1) 205-061       wave washer


In Stockroom 6:
===============
06-11110-01 - electrocraft motor
06-11078-01 - pulley  (for motor)

                                                     BJ
45.55Motor replaced and old spindle installedSUBPAC::BJUBINVILLENFD Fire - RescueSat Nov 25 1995 05:1912
    
    
          I replaced the motor.  I rebuilt the spindle and
     shaft assembly.  The bearings are shot and hummmm at
     the high speed of 1800 RPM's which is the final step
     of the spin process.  The bearings will get hot and 
     won't last.  The bearings also cause some extra vibration
     in the tool.  The entire spindle assembly is coming in 
     on either Monday or Tuesday.  PLEASE use SCRUB.A1 as little
     a possible.  If both scrubbers are free, use #2.

                                           BJ
45.56spin station bluesSUBPAC::LANDRYSat Nov 25 1995 18:3017
    The Spin Station shaft assembly was received in today.  Due to
    manufacturing constraints, the system wasn't relinquished to us.
    Therefore, the assembly is located in the large compartment of the 
    grey roll-around tool box, should the system become available.  By
    the way, the assembly arrived fully assembled, not in the many pieces
    we feared it would show up as.  
    
    Mid-afternoon, the system went down for a "robot fingers not closed"
    error.  One of the grippers on the robots left arm was making contact
    with the spin station fingers.  This was prohibiting it from picking
    the wafer up properly.  Adjusted the spin station lock position such
    that the robot grippers clear the spin station fingers.  After this
    was achieved, the robot was "bouncing" at the wafer grip position.
    Re-taught the grip position and the system ran fine.  
    
                                    		Weekend warriors
    
45.57New Spindle installed, not quite up yetSUBPAC::LANDRYSun Nov 26 1995 19:1727
Today, the new spin station spindle assembly was installed in the system.
Many assembly learning curves along the way.  Many post adjustments needed
by the end of installation.  Probably not recommended for a one man job.
And still, the system is down, for no motor rotation.  

After removing the old assembly, it was evident that the tools to properly
construct/install the assembly don't exist in CMP.  Some hardships were
fitting the new bearing into it's retaining cavity (PVC pipe had to assist
on this one), Allen wrenches too tall, wrenches turning constraints, etc.

Anyway, everything finally came together mechanically.  Had to adjust the 
spindle height, had to adjust two sensors that apparently got knocked out 
of position a bit,  had to replace a broken micro-switch for the spin 
fingers closed position.  Those are all set now.

So, the current status is that the spin motor won't rotate.  I see that the
inhibit switch is active, which I believe prevents the motor from receiving
power.  Hopefully, there is info in the manual.  I had talked with Ron
Simmons earlier in the evening.  He says to look at a possible bad board
for the motor, but I hadn't noticed the inhibit LED on at the time.  You
may want to consult him before you get too deep.  He mentioned a PIA board
but reconfirm with him that this is the case.

Thanks go to Jesus Roa for his help with a lot of the installation.  He was
extremely helpful.

      					Doc  
45.58spin station spindle shaftFABSIX::R_GEEMon Nov 27 1995 07:0417
	* Took over for A shift after the spin station shaft was replaced,
	  the motor wouldn't rotate.

	  - Checked the fuses and voltages, all o.k.

	  - Removed the drive belt from the motor and found the motor
	    was working fine.

	  - Noticed there was a mechanical bind in the spin station shaft.
	    Removed the shaft and found the bottom of the finger assembly
	    rubbing against the top of the bellows, adjusted and 
	    re-assemblied.

	  - Calibrated the spin station spin speed and adjusted some
	    sensors, all set.
	 
					B shift 
45.59rebuilt spin station shaftSTRATA::RIDLONEliminate the obviousTue Nov 28 1995 00:423
    Rebuilt the spin station shaft assembly with bearings found in stock.
    Wanted to see if we could rebuild them without a press. Only took about
    an hour and end result is as good as new.
45.1SCRUB.A1 INSTALL/MECHANICAL ACCEPTANCESUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 01 1995 23:24253
SUBPAC::LANDRY                                       10 lines   6-JUN-1994 16:56
                                -< 6/6 update >-
--------------------------------------------------------------------------------
    All,
    
    KSI (the plumbing contractors) has been diligently working on the
    installation of the exhaust/drain configuration.  Yes, the drains and
    the exhaust end up going out the same plumbing.  What they have done
    is run plumbing up to the system.  They seemed to be moving along.
    
    No other hookup activity was noticed today.
    
                                                     Doc

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Note 65.2                         CMP-SCRUB.A1                          2 of 145
SUBPAC::LANDRY                                       25 lines  16-JUN-1994 16:04
                                -< 6/16 Update >-
--------------------------------------------------------------------------------
    Installation Update:
    
    The GCW drain sections have been completed.  They still need to tie
    them into the exhaust.  Said exhaust has yet to be run.
    
    The Ammonium Hydroxide line has been installed.
    
    The High Purity DI lines have been run.
    
    The electrical is complete.  They just had to supply a 120 VAC outlet.
    
    The rack for the OCP's has been constructed and the OCP's have been
    mounted.  Awaiting hook up of the communication line to the main
    system.
    
    Earl Dawson and I brought up all the accessory equipment related to
    this system.  The "touch screen" monitor has been installed and one
    of the smoked grey covers has been installed.  Still need to attach 
    the last remaining cover.  Will have to procure some hardware to
    accomplish the feat.
    
    The spare parts have been identified and stockroom personnel have full
    control over them at this time.
    
    						Doc

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Note 65.3                         CMP-SCRUB.A1                          3 of 145
SUBPAC::LANDRY                                       16 lines  24-JUN-1994 14:12
                         -< 6/24 Installation Update >-
--------------------------------------------------------------------------------
    *  GCW drains complete
    
    *  NH4OH line complete
    
    *  UHPDI 75% complete
    
    *  Electrical complete
    
    *  Electrical for the OCP's is complete.  Still need to have OCP comm
       line to the system connected.
    
    *  Still waiting for exhaust work to begin
    
    *  Installed final smoked grey cover
    
    						Doc

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Note 65.4                         CMP-SCRUB.A1                          4 of 145
SUBPAC::TOOKER                                       24 lines   8-JUL-1994 11:03
                         -< Hook-Up Status For 7/8/94 >-
--------------------------------------------------------------------------------
                CMP_SCRUB.A1 Tool Hook-Up Status For 7/8/94



COMPLETED ITEMS:
----------------

    *  DI Water connections

    *  Ammonium Hydroxide connections

    *  All GCW drain connections

    *  Eelectrical connections


OPEN ITEMS:
-----------

    *  CDA final connection

    *  All exhaust work

    *  OCP interface to system

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Note 65.5                         CMP-SCRUB.A1                          5 of 145
SUBPAC::TOOKER                                       14 lines  26-JUL-1994 09:20
                                    -< ex >-
--------------------------------------------------------------------------------

                CMP-SCRUB.A1 Tool Hook-Up Status As Of  7/25/94


PUNCH LIST ITEMS
----------------

             ITEM                                      RESPONSIBLE PERSON
   --------------------------------------------------------------------------

  1) Complete exhaust work.                            D. Atkinson/NEEVCO

  2) Install additional pipe                           d. Atkinson/NEEVCO
     support on exhaust.

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Note 65.6                         CMP-SCRUB.A1                          6 of 145
SUBPAC::LANDRY                                        9 lines   1-AUG-1994 13:14
                     -< 8/1 equipment installation update >-
--------------------------------------------------------------------------------
    Brian and I ran the tubing and hooked up the CDA to the system.  This
    completes all the plumbing hookups to the system.  The only remaining
    hook up concerns the communication connection between the main system
    and the OCP.  
    
    We also repaired the magnets on the plexiglass access doors.  The
    magnets had become unglued from the plexi........so we reglued them!
    
    						Doc

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Note 65.7                         CMP-SCRUB.A1                          7 of 145
SUBPAC::BJUBINVILLE                                  16 lines   2-AUG-1994 16:42
                         -< Ron Simmons has arrived!! >-
--------------------------------------------------------------------------------
    
    
    
        Ron Simmons was in this afternoon so here's the scoop.
    The facility guys were turning on the N2, DI water and CDA when
    they discovered some leaks near CMP.A1 so the scrubbers were
    on hold.  Ron will be back in the morning around 8am to start
    things into purge.  The power is all hooked up but the 15A
    breaker is off on both machines.  There was a concern with a
    fitting on the 1/2" ammonium line.  Ron Simmons would rather
    not use stainless.  He doesn't need the fitting to put the
    machine into purge so he'll bring the fitting/parts with him
    on Monday.
    
    
    BJ

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Note 65.9                         CMP-SCRUB.A1                          9 of 145
SUBPAC::BJUBINVILLE                                  11 lines   9-AUG-1994 16:02
                            -< we're getting there >-
--------------------------------------------------------------------------------
    
    
        Ron I and worked with the wafers on this scrubber
    today.  There was a screw on the spin station carriage
    plate that must of broken off during shipping.  We also
    realigned the robot transfer arm for a smoother pick-up.
    The brushes were installed as well.  We are going to purge 
    the NH4OH with DI in the morning.  We cycled through (50)
    wafers without any problems.
    
                                                   BJ

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Note 65.10                        CMP-SCRUB.A1                         10 of 145
SUBPAC::BJUBINVILLE                                  10 lines  10-AUG-1994 16:14
                               -< 8/10 passdown >-
--------------------------------------------------------------------------------
    
    
      The guys downstairs wanted the ammonia line flushed with DI
    water for 24 hours and the pressurized N2 after that.  I have
    this scrubbed in full purge as of right now.  I'm take a 1/2
    day tomorrow so I'll be filling Doc in on where and when with
    the N2.  Ron came in this morning and tied up some loose ends 
    and to make everything was ok, which it was.
    
    BJ

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Note 65.11                        CMP-SCRUB.A1                         11 of 145
SUBPAC::LANDRY                                       12 lines  11-AUG-1994 19:08
                          -< purged and purified!!! >-
--------------------------------------------------------------------------------
    The H20 Purge on the ammonium Hydroxide line was completed at 3:00 PM.  
    The N2 purge on the line was then started and completed.  The NH4OH
    line was then re-attached to it's proper port.  We could possibly see
    NH4OH to the tool as soon as Friday.
    
    We still need to have the OCP's interfaced to the main system
    
    We attempted to run the systems today with a "burn-in" recipe.  The
    system expirienced several timeout/sensor problems.  The rep will
    be in to address the systems on Friday.
    
                                                    Doc

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Note 65.18                        CMP-SCRUB.A1                         18 of 145
SUBPAC::BJUBINVILLE                                  23 lines  22-AUG-1994 17:01
                             -< Passdown for 8/22 >-
--------------------------------------------------------------------------------
    
    
         The problem with the outter brush seems to have been fixed
    after Ron replaced the amplifier and A2 PIA chip.  The machine
    is back on track with 150 wafers through it towards its 1000 wafer
    goal. 
        
         The OCP interface that was designed for us through OnTrak
    seems to be wrong.  Their schematic seems to have been misplaced
    so another one is being faxed to us tomorrow.  We will be evaluating
    this further tomorrow.  Jim T. will be looking the original specs
    that DEC layed out to OnTrak for our request.
    
         The ammonia needed to be regulated at 35psi. but it was never
    done.  Dan Smith is looking to get me a teflon regulator and teflon
    gauge in the morning.  Unregulated, it will be around 45-50psi.
    
         The DI water pressure was still sitting around 30psi at 3:30pm
    today.  Bob Kerwin did come into CMP to look at the gauge but it 
    remains to be unseen if anything was accomplished beyond 3:30pm.
    
    
    BJ
45.2COMPUTER INITIALIZATION PROBLEMSSUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 01 1995 23:2438
SUBPAC::BJUBINVILLE                                  35 lines  15-AUG-1994 18:07
                             -< Passdown for 8/15 >-
--------------------------------------------------------------------------------
    
    
    
    *  Ron and I came into where the SCRUB_A2 was stopped and had
       homing problems.  After we rebooted the machine, there was 
       a problem on boot up.  The machine is suppose to go right 
       into the OnTrak self initializing mode but it was staying 
       at the WinShell prompt.  After Ron called the software
       guru from OnTrack he had use copy a file over from another
       directory.  These machines are touch screens so we had to hunt
       down a keyboard with a RS232 connector.  We had to type the 
       following as these machines are not DOS operated.
    
         WinShell:> COPY DATA2 DATA -R
    
       After this is typed, reboot the machine it ok.  Every 2 minutes
       the machine does a self back-up of essential data files that usually
       takes a couple of milliseconds.  If you get acurate enough, if you
       shut the machine the exact same time as this back-up starts, the
       machine will put all of the robot offsets reset to factory defaults.
       OnTrack said this has only happened twice in our model history.  
       This is very rare.  I copied the offsets for both machines into
       their respective logbooks.  I will eventually copy them into here.
    
    *  The DI water is still an issue.  I spoke with Bob Kerwin and
       the issude is still being addressed.  He's looking at least
       another week before we some action.
    
    *  Repaired a few more leaks
    
    * we went over some maintainence training as well as some process
      issues with Steve.
    
    BJ
        
45.3FLOW VALVE WON'T ADJUST HIGHER, MOTOR SPEED OUT OF SPECSUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 01 1995 23:2622
SUBPAC::BJUBINVILLE                                  23 lines  16-AUG-1994 13:10
                             -< Passdown for 8/16 >-
--------------------------------------------------------------------------------
    

          We calibrated the motor speed offsets to match the
    "Burn-In" recipe.
    
          We found the outter bottom brush flow valve not reaching
    over 400ml, it should of been higher.  We replaced the valve and
    found a defect in the valve.  We borrowed on from the Wet-Lab
    and got this this one going.  Ron will bring the borrowed parts
    to get the one in the Wet-Lab ready.
    
       The machine has continued to be in mechanical acceptance
    and has gotten up to around 700 wafers now.
    
                                              BJ
          This machine is still in the 1000 maintainence
    acceptance.
    
                                    BJ 
45.4SENSORS AND MOTOR SPEED PROBLEMSSUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 01 1995 23:2750
SUBPAC::BJUBINVILLE                                  24 lines  18-AUG-1994 16:24
                             -< Passdown for 8/18 >-
--------------------------------------------------------------------------------
    
    
    *  We finally ironed out the bugs.  The was sensor problem
     with the inside brush station.  The alarm kept tripping
     because the sensor would detect a wafer but would stay
     on instead of shutting off.  We traced it back to a 3v
     drop across the sensor/amplifier.  We replaced the IC 
     chip for this sensor and the voltage got back up to 5v.
    
    *  We set the brush height to 14.5mm pending results from
     Tencor.  We might have to either raise or lower them.
    
    *  We tweaked in the outside, inside and spin motor speed
     offsets to stablize them. 
    
    *  The receiver door switch had the same problem as #2 yesterday.
     The LOCKED and UNLOCKED lights stayed lit when only the LOCKED
     was suppose to.  We had to adjust the sensor.
    
    
    We've run about 150 wafers straight with now problems.  Keep
    your fingers crossed.
    
    BJ 

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Note 65.15                        CMP-SCRUB.A1                         15 of 145
SUBPAC::BJUBINVILLE                                  15 lines  17-AUG-1994 17:27
                             -< passdown for 8/17 >-
--------------------------------------------------------------------------------
    
        The initial problem was that the robot wasn't picking
    up the wafer properly.  We retaught the robot position to
    get in.    
        A "inside brush motor speed out of spec" error was coming up
    all the time.  We traced it to the drive belts on the rollers.  
    We tightened them up and the motor feed back was stable but just
    a few RPM's under 40.  We are going to tweak it to 40 tomorrow.  
    There also seems to be a problem with the inside brush sensor.  Ron
    replaced the PIA #1 board to try and get it to behaive.
    
    BJ
    
                                                        BJ
    
45.5SEALS REPLACED, LEAKING MANIFOLDS AND MOTOR SPEEDSSUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 01 1995 23:2818
SUBPAC::BJUBINVILLE                                  15 lines  25-AUG-1994 17:02
                             -< Passdown for 8/24 >-
--------------------------------------------------------------------------------
    
    
      *  Inner brush rear roller shaft was leaking, replaced
         seal    
    
      *  Outer brush rear roller shaft was leaking, replaced
         seal    
    
      *  Outer exit manifold leaking out end (brush lift end),
         replaced manifold.
    
      *  tweaked in inside, outside and spin motor speed offsets
    
    
    BJ
45.6CARRIAGE PROBLEMSSUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 01 1995 23:2826
SUBPAC::LANDRY                                       22 lines  20-SEP-1994 14:53
                          -< Get a "grip" on it man! >-
--------------------------------------------------------------------------------
    Today..........
    
    *  The system shattered a wafer.  First off was to clean the big mess
       it made.  Picked up as many pieces as possible by hand and disposed
       of them in the proper recepticle.  Removed the remaining fragments
       by use of the hose vacuum.  Wiped down affected surfaces.
    
    
    *  Traced the problem to be with the retracting roller assembly NOT
       being level.  As the grippers came in to hold the wafer, it didn't
       secure it properly.  Of course I didn't see it actually happen or I
       would have stopped it before it broke the wafer.  But, through
       monitoring it's performance on the next several wafers, I was able
       to see this almost happen again.  Found the roller assembly bracket
       to be loose.
    
    *  Jim T. and myself then manually operated the system to align the
       roller assembly properly and then secured the bracket back to it's
       optimum operating setting.
    
                                                 Doc
    
    
45.7AMMONIA TURNED ONSUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 01 1995 23:2921
SUBPAC::LANDRY                                       18 lines  30-SEP-1994 14:29
              -< Is that a babies diaper?  No, thats the NH4OH! >-
--------------------------------------------------------------------------------
    *  AMMONIA IS FLOWING!
    
    *  The lockout/tagout has been removed from the 2% NH4OH line.
    
    *  We (Jim Sadin and myself) edited a program to get the NH4OH to flow.
       The internal shut off valve (or turn on valve to some) was opened,
       the flow meters for were opened/adjusted, and the lines were
       observed for leaks (no leaks found).
    
    *  We did a quick D.O.E. for NH4OH flow with both systems A1 & A2
       running at the same time.  We were capable of attaining flows of
       7-8 on the flow meter.  Both systems fluctuated periodically.
    
    *  The programs were returned to their normal settings for NH4OH, 
       which is 20 seconds for the outside brush and 10 seconds for the
       inside brush.
    
    						Doc
45.8SOFTWARE UPGRADESUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 01 1995 23:3016
SUBPAC::BJUBINVILLE "Quit crying and play hockey!"   13 lines   7-OCT-1994 15:58
                             -< Passdown for 10/7 >-
--------------------------------------------------------------------------------
    
    
      Ron came in and completed yet another software
    upgrade to this machine.  It was designed to 
    eliminate some small bugs that were irrevalent
    to us but none the less, they're gone.  The
    new rev. # is listed in the book.
    
      Ron also replaced the (4) spin station fingers
    to a bigger style with better wafer handling.
    Wafers were run through without any problems.
     
    BJ
45.9DOUBLE STACKED WAFERSUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 01 1995 23:3120
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SUBPAC::BJUBINVILLE "Quit crying and play hockey!"   14 lines  13-OCT-1994 16:09
                            -< Passdown for 10/13 >-
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       The RECEIVER access door was opened during the run causing
    the machine to stop.  There was a wafer in the otter brush
    that wasn't recovered when someone RESET the station.  The
    next wafer through piggy backed through the rest of the
    cycle.  If you want to reset a station and there is a wafer
    in that station, recover the wafer FIRST.  If you don't,
    when you RESET the station, you are just telling the machine
    there is now no wafer in the station when there really is.
    Thus.... piggy back.....
    
    BJ
45.10HEAT LAMP NOT COMING ONSUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 01 1995 23:3112
SUBPAC::BJUBINVILLE "Quit crying and play hockey!"    9 lines   2-NOV-1994 16:23
                             -< Passdown for 11/2 >-
--------------------------------------------------------------------------------
    
    
       The lamp wasn't coming during its cycle.  The lamp
    was in the socket but wasn't making good contact.  I
    believe it was due to vibration in the room.  I will
    start to look into getting some kind of a clip to hold
    it into place.
    
                                              BJ
45.11BRUSH CHANGESUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 01 1995 23:3123
SUBPAC::LANDRY                                       20 lines   8-NOV-1994 16:47
               -< Bald people shouldn't have to do brushes!!!! >-
--------------------------------------------------------------------------------
    Todays activities.......
    
    What a day!  Ron Simmons came in today to assist in changing out the
    PVA brushes on the system.  We started about 10:30 AM and just finished
    up at 4:30 PM.  We definitely had some big learning curves!  Let me
    explain.
    
    First off, the brushes were extremely difficult to install onto their
    cores.  The PVA material is easily stretched and the studs are easy 
    damage.  The brush must be put onto the core evenly.  This proved to be
    the biggest problem with the installation.  Bobby, Steve and myself all
    to a crack at putting these brushes onto the core.  I'd say all three
    of us didn't fair to well.  Although the brushes were installed to what
    we thought to be pretty good, we were proven wrong upon core
    installation.  The peaks and valleys were not evident until the brushes
    /cores were rotated.  So off they came again to be retried.  Finally,
    many hours later, the brushes were installed properly.  Steve will now
    begin to perform particle checks.  Lets hope all is well.
    
    						Doc  /  Bobby
45.12MEGASONIC SWEEPSUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 01 1995 23:3213
SUBPAC::BJUBINVILLE "Quit crying and play hockey!"   10 lines  10-NOV-1994 11:31
                            -< Passdown for 11/10 >-
--------------------------------------------------------------------------------
    
         Engineering was inquiring on the dwell time
    on the megasonic sweep.  We looked into the LOW
    and HIGH flow sensor settings and the window was
    smaller than A2.  We brought them to the same setting.
    Another thing was the megasonic flow was at 800ml.  
    We matched it at 900ml like A2 as well.  The dwell is
    very minimal and acceptable at this time by Engineering.
    
                                            1ft shift boys
45.13WAFER ROLLER NOT SPINNINGSUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 01 1995 23:3210
ASDG::POIRIER                                         7 lines  22-NOV-1994 23:25
                     -< Guide rollers in brush station #2 >-
--------------------------------------------------------------------------------
    
    * Jim Sadin noticed that the wafers were not spinning in brush station #2.
      Bob and I tightened the set screws on the guide rollers and the
      wafers now spin normally. It appears that the rollers were slipping on
      the drive shafts.
    
                                                                    John.
45.14SUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 01 1995 23:328
PATE::GEE                                             5 lines  28-NOV-1994 23:35
                        -< Outside station lower brush >-
--------------------------------------------------------------------------------
    The outside station lower brush had some hesitation as it rotated in
    idle speed. Installed a missing bearing that sits inside the brush 
    core end from stock.
       
    Bob
45.15ROBOT PROBLEMSSUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 01 1995 23:3317
SUBPAC::LANDRY                                       14 lines   1-DEC-1994 17:02
                       -< Who needs a wafer dicing saw? >-
--------------------------------------------------------------------------------
    Today, the robot malfunctioned, breaking a wafer (exercise wafer) very
    neatly in two half moon pieces.  It broke so cleanly that one half
    actually stayed positioned in the robot fingers.  How it broke is a bit
    sketchy!  The robot picked up the wafer from the spin gripper.  It is
    believed that the robot didn't properly rotate 90 degrees prior to
    attempting it's move to the unload station.  The robot was found with
    it's finger (be nice here) up against the plexiglass cover. 
    
    The system was EMO'd when the breakage occured (good quick judgement).
    Upon repowering the system, all stations were initialized.  Ran several
    tests wafers to confirm problem had vanished.  We'll have to keep an
    eye on this for a bit.
    
    						Doc 
45.16INSIDE BRUSH TIMEOUT ERRORSUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 01 1995 23:3415
SUBPAC::BJUBINVILLE "Quit crying and play hockey!"   12 lines   7-DEC-1994 14:32
                             -< Passdown for 12/7 >-
--------------------------------------------------------------------------------
    
    
       The scrubber kept going into CLEARING after every
    three wafers.  Machine would alarm and say the scrubber
    timed out looking for the wafer at the inside brush 
    station.  If an error involving any station timeouts
    or lost/broken wafer, there's a good chance you'll
    need to RESET the receiver.  When you reset the receiver,
    the computer re-sync's the counters which gets all of the
    stations on the same time plane.  
    
                                               BJ
45.17ROBOT PROBLEMSSUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 01 1995 23:3416
SUBPAC::BJUBINVILLE "Quit crying and play hockey!"   13 lines   9-DEC-1994 11:46
                             -< Passdown for 12/9 >-
--------------------------------------------------------------------------------
       
       Ron came in for a visit.  I told him about the
    two wafers that broken in the last two weeks.  We
    went over the robot and spin station and found some
    problems.  When the spin station first grabs the wafer,
    it closes twice to take the wafer.  We found there was
    lack of air pressure to take the wafer on all four
    fingers.  After we adjusted the air to the fingers,
    it grabbed fine.  The robot fingers weren't closing
    all the way either, same fix.  We bent the tabs in 
    on the lamp socket so the lamp will hold tighter.
    
                                         BJ
45.18SQEALING NOISE, BRUSH ROTATION HESITATIONSUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 01 1995 23:3526
          <<< ASDG::DISK$SYS_DATA:[NOTES$LIBRARY]FILMS_ONLY.NOTE;1 >>>
                                -< Films Only! >-
================================================================================
Note 65.54                        CMP-SCRUB.A1                         54 of 145
SUBPAC::BJUBINVILLE "Quit crying and play hockey!"   19 lines   3-JAN-1995 07:02
                             -< Passdown for 1/3 >-
--------------------------------------------------------------------------------
    
    
       I went through with some things with Bob concerning the 
    
    squealing noise coming from the upper brush supporting mounts.
    
    We re-aligned the supports to get the noise to go away.  Bob
    
    also noticed that the lower brush on both stations seemed to
    
    be stopping and hesitating.  We traced it to the front bearings
    
    on both brushes.  We replaced them and everything ran fine.  There
    
    are no more bearings in stock.  I put in a shortage request as well
    
    as up-ing the min/max level to 16 bearings.
    
                                                BJ
45.19BLADE LIFTER NOT REPEATINGSUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 01 1995 23:3739
SUBPAC::BJUBINVILLE "IT'S HOCKEY TIME!!"             10 lines   2-FEB-1995 09:52
                   -< Split Ends, isn't that a hair thing? >-
--------------------------------------------------------------------------------
      
          This morning, Ron Simmons came to look at our
    blade lifter issue.  It was traced to the drive chain
    for the lifter.  In one section, it was split up the middle 
    for about an inch.  The split in the belt during the travel
    wasn't as effective as when the split got the bottom pulley,
    it was right when the blade was at its top position.  This
    is where it was not repeating.  The belt is getting replaced
    within the next half hour.
                                                   BJ and Doc

          <<< ASDG::DISK$SYS_DATA:[NOTES$LIBRARY]FILMS_ONLY.NOTE;1 >>>
                                -< Films Only! >-
================================================================================
Note 65.64                        CMP-SCRUB.A1                         64 of 145
SUBPAC::LANDRY                                       18 lines   1-FEB-1995 18:31
                         -< Whats up with the Knife? >-
--------------------------------------------------------------------------------
    The system is currently down for a robot to knife transfer problem.
    The blade isn't returning to it's proper receive position everytime.
    The cassette indexing isn't consistant either.  It has double loaded
    wafers in the same cassette slot.  This means that the cassette index-
    ing is moving enough to clear the inhibit position, but not far enough
    to make it to the next slot.  Once this happens, the cassette homes,
    even though there are more wafers coming through the line.  Bizarre!
    The problem appears to be a PC board problem.  Bobby Gee and I swapped
    out the Intellegent Stepper/Driver board with one from stock.  This
    board controls both the knife and cassette indexing.  No luck.  Next
    most possible culprit is the PIA board.  This board, once installed,
    will require calibration.  Possible mechanical problems with the unload
    station are remote, but still possible.  Good Luck.
    
    Ron Simmons can be in tomorrow morning if needed.  He will call us in
    the AM.
    
    						Doc
45.20BRUSHES WON'T ROTATE IN IDLESUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 01 1995 23:379
PATE::GEE                                             6 lines   2-FEB-1995 23:21
                               -< Scrub Station >-
--------------------------------------------------------------------------------
	The brushes would not rotate in Idle mode. Found that the 
	wrong process program was loaded. Loaded the correct program
        "STRAS_CLEAN_BEST", System is working fine.


						John & Bob
45.21SUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 01 1995 23:37204
SUBPAC::BJUBINVILLE "IT'S HOCKEY TIME!!"            201 lines   6-FEB-1995 01:48
                   -< Machine Characterization as of 2/6/95 >-
--------------------------------------------------------------------------------
   
                              CMP_SCRUB.A1
                        ONTRAK DSS-200 SCRUBBER
               MACHINE MAINTENANCE CHARACTERIZATION SHEET

LOAD AREA
==========

                                             ____
ELEVATOR: PHYSICAL POSITION                  ||_| <-- (1)
          (measurement taken from (1)top     ||    ^
          of the elevator mounting           ||    ^
          bracket to the (2)bottom of the    || | <-- (2)
          motor mount casing.                ||||_____ <--elevator base
           
 

                                UPPER POSITION (SLOT #1)  -- 1 27/32"  

                                HOME POSITION -- 1 3/16"

                                LOWER POSITION (SLOT #25) -- 7 13/16" 


MACHINE OFFSET --  (found in ROBOT OFFSETS menu)
                   
                                 LOAD STATION --  1310
  
              

SPRAY MAINIFOLD --  
(bar and nozzle position)      verify alignment of scribed marks

============================================================================

SCRUB MODULES
=============


MICROMETER SETTINGS:  verify ENGINEERING set point

                                 INSIDE BRUSH STATION | OUTSIDE BRUSH STATION
                                    SETTING/ACTUAL    |     SETTING/ACTUAL
                                 --------------------------------------------
                                                       |
WAFER ROTATION (TACH READING IN RPM'S)  40    /  44    |   50      /    49.5
                                                       |
BRUSH ROTATION (TACH READING IN RPM'S) 118    /  118   |   118     /    121


SPRAY MAINIFOLD --  
(bar and nozzle position)      verify alignment of scribed marks

==============================================================================

SPIN STAION
===========
                                            SETTING/ACTUAL 
                                            --------------
                        
WAFER ROTATION (TACH READING IN RPM'S)        1800 / 1715     

                                               500 / 569


CUP HEIGHT -- (measurement taken         UPPER POSITION -- 7 9/16"        
              from very top of any     
              finger to bottom of        MIDDLE POSITION -- 6 15/16"
              tub)
                                         LOWER POSITION -- 4 7/16"


GRIPPER FINGERS -- (measurement taken          FINGERS OPEN -- 8 1/2"
                   from center of left 
                   rear finger to center       FINGERS CLOSED -- 7 1/2"
                   of left front finger)


WAFER TEMPERATURE --  AS WAFER ENTERS SPIN STATION  -- 75 F

                      AS LAMP IS ON  -- 80 F

                      AFTER LAMP SHUTS OFF  -- 75 F


EXHAUST VELOCITY (in inches) -- 1.3


============================================================================

ROBOT
=====

OFFSETS --     WRIST AT SPIN STATION    --  108

               WRIST AT RECEIVE         --  240

               SPIN XPORT DELAY         --  40

               ROTATION AT SPIN STATION --  882

               ROTATION AT RECEIVE      --  1813

               ROBOT FINGERS            --  370


ROBOT FINGERS -- (measurement taken         OPEN -- 9 7/16" 
                 from O.D. to O.D.
                 from finger to finger      CLOSED -- 8 1/4"


==========================================================================

UNLOAD MODULE
=============


CASSETTE AT POSTION SLOT #1-- (insert new cassette
                              and let machine go to
                              position and slot #1.     --  16 3/4"
                              measure from the outer
                              most part of the back
                              panel the middle of slot
                              #1)
                               

KNIFE EDGE -- (measure from very         UPPER POSITION -- 10 1/4"
              top of knife to the
              top of panel that the      LOWER POSITION -- 7/8"
              edge goes into)



MACHINE OFFSET --  (found in ROBOT OFFSETS menu) 
                   
                                UNLOAD STATION --  490

                                BLADE LIFTER --    11500

=============================================================================

ELECTRONICS
===========
                                                  IDLE     |   RUNNING
                                                ========================

POWER SUPPLY VOLTAGE --               
                        +5 VOLT POWER SUPPLY       5.15    |   5.15
                                                           |
                        +12 VOLT POWER SUPPLY      12.3    |   12.37
                                                           |
                        -12 VOLT POWER SUPPLY     -12.38   |   -12.38  
                                                           |
                        +24 VOLT POWER SUPPLY      24      |   24
                                                           |
                        +48 VOLT POWER SUPPLY      48.2    |   48.2


SERVO DRIVE POWER SUPPLY-     
                   
                        +40 VOLT PICK-OFF          41      |   41	

                        +5 VOLT PICK-OFF           5       |   5


============================================================================

FLOW SETTINGS
=============

                                     SEND --  5

                  AMMONIA OUTSIDE STATION --  3

                      OUTSIDE BRUSH UPPER --  10

                      OUTSIDE BRUSH LOWER --  7

                   AMMONIA INSIDE STATION --  3

                       INSIDE BRUSH UPPER --  9

                       INSIDE BRUSH LOWER --  7

                       SPIN STATION UPPER --  3

                       SPIN STATION LOWER --  3

                        MEGASONIC NOZZLE  --  9

===========================================================================

PRESSURE SETTING                                50  PSI
================


SIGNET FLOW SETTING
===================                         LOW --  40

                                            HIGH -- 0

45.22SUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 01 1995 23:3715
SUBPAC::LANDRY                                       12 lines  13-FEB-1995 17:11
                         -< New Software installed.   >-
--------------------------------------------------------------------------------
    Ron Simmons came in a started performing a couple of up-grades to the
    system.  New software was installed and checked out.  The new software
    will protect all data entry regardless of when the system is shutdown.
    The old version didn't have this feature and it took several hours to
    re-enter all the datat once it was lost, ask Brian, he'll tell you what
    he went through the time this happened to us.  
    
    Ron has a couple of more items to perform when he and the system are
    both available.
    
    							Doc
    
45.23coiled electrical cord for the send station elevator SUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 01 1995 23:3839
SUBPAC::LANDRY                                       12 lines  22-FEB-1995 16:35
               -< Minor problem needs to be addressed w/ Ontrak >-
--------------------------------------------------------------------------------
    The coiled electrical cord for the send station elevator has been
    chaffed conciderably.  It was beginning to create particles on the 
    outside of the plexiglass box (no contamination within the box where
    the wafers are loaded).  As a temporary provision to stop this from
    happening, a strand of electrical tape was applied.
    
    OnTrak will be notified of the problem.  We'll get the cords replaced
    as well as possible changing the "style" of hardware that protrudes
    from the plexiglass box.  It currently has hex-head hardware where a
    button head style would probably work out better.  Stay tuned!
    
    						Doc

          <<< ASDG::DISK$SYS_DATA:[NOTES$LIBRARY]FILMS_ONLY.NOTE;1 >>>
                                -< Films Only! >-
================================================================================
Note 65.86                        CMP-SCRUB.A1                         86 of 145
SUBPAC::LANDRY                                       16 lines   7-APR-1995 14:14
                           -< wire harness replaced >-
--------------------------------------------------------------------------------
    Ron Simmons, OnTrak Rep Extraodinaire, came in today to replace the
    wiring for the Load Staion elevator power.  The original wiring was
    mounted such that the wiring would rub against the hardware protruding
    from the load station tub.  The new wiring has been installed such that
    it will no longer rub in the previous manner.  The socket head screws
    will be replaced in the near future to button head screws, hence
    preventing this chaffing to occur again.
    
    We also checked out the possible leak on the feedthroughs in the brush
    stations.  Water was noticed to have formed there on one of his
    previous visits.  The last two times he was here, they have been dry,
    as should be.  Original sighting could have possible been attributed to
    wet transfer boats, as they are some times temporarily placed there.
    We'll monitor for future sightings.
    
    						Doc
45.24HOT DI WATER TIE INSUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 01 1995 23:3816
SUBPAC::LANDRY                                       13 lines  23-MAR-1995 17:07
                   -< Sometimes its hot sometimes its not! >-
--------------------------------------------------------------------------------
    Heres what we got.......
    
    	The Hot DI water loop hookup has been performed.  The system
    now has the capability to dispense hot or cold water.  Currently,
    the cold (not really cold, but the regular di water normally going
    there) is turned on to the system.  The Hot loop's valve has been 
    locked out /  tagged until it is ready to use.  Each input line is
    equipped with a temperature gauge.
    
    	The status of the equipment at this time remains as VERIFY, on
    	account that we gotta make sure the particle counts are acceptable.
    
    						1st Shifters  
45.25SUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 01 1995 23:3917
SUBPAC::LANDRY                                       14 lines  24-MAR-1995 17:29
                         -< Hot DI Water Loop Status >-
--------------------------------------------------------------------------------
    The lastest scoop on the Hot Di Hookup goes like this.........
    
    	We coordinated some work today with Holden Mechanical.  They had
    introduces water into the Hot DI line, when in fact, we weren't ready
    to receive it.  Therefore, we had them disconnect a fitting in the Sub
    Fab to drain the line to the system.  Then Roger and I hooked up an
    N2 purge to the line to dry it out.  After many hours, Holden checked
    the line at their end.  They still found traces of moisture. Therefore,
    it was decided that we would leave the N2 purge on until the line was
    completely dry.  Holden will periodically check the status and let us
    know when all is dry.
    
    						Doc  /  Roger
    
45.26SUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 01 1995 23:399
ASDG::COOPERMAN                                       6 lines  25-APR-1995 13:22
                           -< water flow adjustment >-
--------------------------------------------------------------------------------
    
    Adjusted flow for top brush on .a1 to 9 from ~5-6. Should
    	have been at 9, not sure why was low.
    
    Steve
    
45.27SUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 01 1995 23:3912
SUBPAC::BJUBINVILLE "NFD Fire - Rescue"               9 lines  26-APR-1995 10:50
                  -< PVA brushes replaced and being aligned >-
--------------------------------------------------------------------------------
    
    
           Machine ended up failing MQC's for high particles.  It
    was either leave it down or try changing them.  After they were
    changed, the scrubber came right into spec.  However.... they
    weren't perfectly asymmetrical.  With Larry and John, we gave
    it another shot.  They are coming in nice.  They should be finishing
    up real soon.  
                                              BJ
45.28SUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 01 1995 23:399
SUBPAC::BJUBINVILLE "NFD Fire - Rescue"               6 lines  12-MAY-1995 06:23
                         -< Roller speed out of spec >-
--------------------------------------------------------------------------------
    
         Came to a OUTSIDE brush roller out of spec.  This error
     indicates the rollers, not the brushes.  A recalibration was
     performed and the rollers are running fine now without any
     machine errors.
                                         BJ
45.29SUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 01 1995 23:3914
FABSIX::R_POIRIER                                    11 lines  18-MAY-1995 23:52
                         -< Megasonics Sweep Problem >-
--------------------------------------------------------------------------------


There was a problem with the Megasonics Sweep home sensor. We
replaced the Optical Sensor (DEC P/N 94-072339-01) from S/R 94
and Megasonics Sweep Home works fine. Ran 26 dummy wafers to
check out spin station. Particle checks should be run before
using CMP-SCRUB.A1 for product.


					2nd Shift

45.30SUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 01 1995 23:3913
SUBPAC::BJUBINVILLE "NFD Fire - Rescue"              10 lines  30-MAY-1995 07:56
                             -< ROBOT TIMING OUT >-
--------------------------------------------------------------------------------
    
          The system kept alarming because the sensor for FINGERS
        CLOSED wasn't being seen.  After powering down the system
        and removing the covers to the robot, everything was in
        order and working fine.  A dozen or so wafers were run on
        the machine without any problems.  About an hour later, the
        problem came back but was placed in WAFER RECOVERY before I 
        was able to see the problem.  The machine ran fine since.
    
                                                       BJ  
45.31SUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 01 1995 23:3913
    
    
SUBPAC::BJUBINVILLE "NFD Fire - Rescue"               8 lines  23-MAY-1995 06:18
                           -< Megasonic arm linkage >-
--------------------------------------------------------------------------------
    
         The megasonic arm linkage was all out of whack.  After the
      arm was repositioned and the amplifier adjusted it moved fine.
    
        A valve and tee were installed on the DI line for the DI gun
      that will be used only for brush changes.
    
                                                        BJ
45.60ROBOT OFFSETS CHANGEDFABSIX::B_WESTPHALSat Dec 02 1995 17:067
SCRUB.A1 - Down for robot not picking wafers from the spin station.  Found that 
	   the robot fingers were closing improperly around the wafer.  
	   Adjusted the level and positioning of the spin station by adjusting 
	   the 4 base bolts.  Also made several adjustments to the WRIST AT 
	   SPIN, ROTATION AT SPIN, and FINGERS (120,868,210) offsets, ending up 
	   with the final values of 124, 873, and 190 respectively.  Ran a full
	   boat of wafers w/o any problems and returned the tool to production.
45.32ROBOT TIMING OUT SUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 08 1995 22:0013
SUBPAC::BJUBINVILLE "NFD Fire - Rescue"              10 lines  30-MAY-1995 07:56
                             -< ROBOT TIMING OUT >-
--------------------------------------------------------------------------------
    
          The system kept alarming because the sensor for FINGERS
        CLOSED wasn't being seen.  After powering down the system
        and removing the covers to the robot, everything was in
        order and working fine.  A dozen or so wafers were run on
        the machine without any problems.  About an hour later, the
        problem came back but was placed in WAFER RECOVERY before I 
        was able to see the problem.  The machine ran fine since.
    
                                                       BJ  
45.33RECEIVE TIMEOUTS, BRUSH STATION TIMEOUTSUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 08 1995 22:0120
SUBPAC::LANDRY                                       17 lines  30-MAY-1995 18:27
                     -< National Robot Month continues on >-
--------------------------------------------------------------------------------
    A couple of occurances today that required some attention...........
    
    *  With a hot lot running, I was summoned in to look at the system.
       Seems the robot picked up the wafer, then just stalled out.  The
       alarm screen said that the was a timeout looking for the receiver
       cassette.  There was a receiver in there and ready to receive a
       wafer, so I hit start and the run finished fine.  Seems like someone
       may have interrupted the run to fetch some completed wafers in the 
       receiver???
    
    *  Then there was a brush station timeout.  Again, nothing was found to
       be wrong.  Diagnostically reset the station, but couldn't get the 
       load cassette transport belt to turn on.  Had to reboot the software
       to return to normal.
    
    							Doc
    
45.34SYSTEM DOUBLE LOADINGSUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 08 1995 22:0111
SUBPAC::BJUBINVILLE "NFD Fire - Rescue"               8 lines  31-MAY-1995 04:29
                       -< double loading a spin station >-
--------------------------------------------------------------------------------
    
    
         Two wafer got into the spin station at the same time
      for some unknow reason.  Machine had to bew powered down
      for safe removal of the product wafers.  A boat of wafers
      was run without and problems.
    
                                               BJ
45.35WAFER ROLLER ARMS NOT OPENINGSUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 08 1995 22:0215
SUBPAC::LANDRY                                       12 lines  31-MAY-1995 17:55
                            -< Open up them arms! >-
--------------------------------------------------------------------------------
    The system had some timeouts again today...........
    
    Timeout looking for inside brush wafer.  Problem actually is with the
    outside brush station.  When it's time to release the wafer from the
    outside station, the wafer rotation arms were not retracting everytime.
    The bimba shafts for this movement were cleaned and very lightly lube'd
    with a drop of oil (no worry, the bimbas are located outside of the 
    brush stations and pose no contamination threat).  The problem has not
    occured since the lube was placed.
    
    						Doc
    
45.36RECEIVE CASSETTE NOT READY, SENSOR ADJUSTMENTSUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 08 1995 22:0318
SUBPAC::LANDRY                                       15 lines   1-JUN-1995 17:54
                     -< sensor adjustment had to be made >-
--------------------------------------------------------------------------------
    The system came up with a "receiver not ready" (or something close to
    that terminology) error today.  Well, there indeed was a cassette in-
    place and it was ready to receive a wafer.  Went into the I/O functions
    and found that the cassette present sensor was not being made.  Looked
    at the sensor arraingement and found out that the sensor is adjusted by 
    a set screw mounted into the arm above the sensor.  The set screw was
    very loose in the threads of the hole.  This caused the screw to move
    up the threads and out of position.  Adjusted said switch and tested
    results.  All is fine for now.
    
    With the looseness of the set screw, I would not be surprised to see
    this sensor adjustment made again in the future.  Stay tuned!
    
    						Doc
    
45.37ROBOT ARM PROBLEMSUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 08 1995 22:0413
FABSIX::R_POIRIER                                    10 lines  15-JUN-1995 23:43
                             -< Robot arm problem >-
--------------------------------------------------------------------------------


Robot arm kept stopping after picking up a wafer from the
spin station but would not put it in the cassette. This
problem was not constant. Brian found that the load cassette
switch was not being activated all the time when the cassette 
was put in. The set screw had loosened and wasn't making contact.
Tightened the set screw and the problem went away.


45.38ROBOT FINGER PROBLEMSSUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 08 1995 22:0643
          <<< ASDG::DISK$SYS_DATA:[NOTES$LIBRARY]FILMS_ONLY.NOTE;1 >>>
                                -< Films Only! >-
================================================================================
Note 65.118                       CMP-SCRUB.A1                        118 of 145
SUBPAC::LANDRY                                       36 lines  29-JUN-1995 19:46
                         -< Robot Positioning Problem >-
--------------------------------------------------------------------------------
    An educational day..............
    
    	The system robot functions were messed up this morning.  The
    fingers were not closing to their proper position, causing the system
    to "timeout" for finger position.
    
    	Found the several problems with the system.  Problem one was the
    flags for the open + closed potitions were out of whack.  For this fix,
    the open flag must be set up first.  Once done, the motor steps take
    over from there.  The motor steps dictate the position of the closed
    position.  The mechanical flags are only used as indicator for the
    diagnostic menu's.  The closed flag mechanism was then moved to it's
    proper location.  
    
    	After this was setup, we attempted to run some wafers.  We found
    the gripper arms to be over traveling, causing the grippers to flex
    back.  The closed position was re-taught.  Transfered several wafers
    fine, but occasionally, it would mis-grip the wafer.  Upon checkout, 
    we found that the "rotation at spin station" and the "wrist at spin"
    positions were out of tolerence.  These were causing the gripper
    fingers to pick the wafer in the wrong spot on the gripper fingers.
    By this I mean that the wafer was not aligned with the slots on the
    grippers, but instead it was aligned with the shaft.  After the
    positions were re-setup, the system was transfering quite nicely.  
    
    T%he current System Offset settings are:
    
    Load Station  =   1310		Rotation @ Spin Station  =   877
    Unload Station=    490		Rotation @ Receive Sta   =  1813
    Wrist @ Spin Sta = 114 		Balde  =                   11500
    Wrist @ Receive  = 240		Robot Fingers  =             420
    Spin Xport Delay =  40
    
    						Doc  /  Jim T
    
    
45.39BRUSH ROLLER ARM CRACKEDSUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 08 1995 22:0710
SUBPAC::BJUBINVILLE "NFD Fire - Rescue"               7 lines  19-JUL-1995 06:33
                            -< Roller arm cracked >-
--------------------------------------------------------------------------------
    
       Wafers kept sliding by the outside brush station and
     doubling up in the inside brush station.  The right roller
     arm was cracked and causing the roller not to close to stop
     the wafers.  The arm was replaced and aligned.
    
                                                Bob, Leon, BJ
45.40WAFER ROLLER ARMS NOT OPENINGSUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 08 1995 22:0820
          <<< ASDG::DISK$SYS_DATA:[NOTES$LIBRARY]FILMS_ONLY.NOTE;1 >>>
                                -< Films Only! >-
================================================================================
Note 65.122                       CMP-SCRUB.A1                        122 of 145
SUBPAC::LANDRY                                       13 lines  19-JUL-1995 20:10
                            -< roll them arms back >-
--------------------------------------------------------------------------------
    Twice today, the system faulted for a timeout, waiting for a wafer to
    release from the outside brush station.  We found the problem to be
    intermittent.  After several test wafers, the roller arms didn't open
    to allow the wafer to move on to the next station.  The Bimba cylander
    appeared to be a bit sticky.  Cleaned the shaft and lightly lubricated
    using light oil.  Ran several test wafers and it appeared to be smooth.
    
    An hour later, the problem happened again.  Began to run test wafers. 
    No problems occurred.  After 40+ wafers were run through it, the status
    was changed to UP.  We'll have to monitor it to see if further problems
    arise.
    
    							Doc
45.41COMPUTER FREEZE UP, ROBOT FINGER PROBLEMSUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 08 1995 22:0924
SUBPAC::LANDRY                                       21 lines  28-JUL-1995 18:54
                 -< Robot problem solved after a tough fight! >-
--------------------------------------------------------------------------------

      Today, the system had a major problem or two..............

      First off, the computer locked up.  So, it was rebooted and 
      initialized.  All looked well.  Tried running a wafer through 
      the system, but the system came up with a robot malfunction. 
      The open sensor wasn't being made.  Found out that the robot
      was interfered with when trying to prevent a wafer mishap.
      No problem, I'll just reset up the flags/robot positions.
      Nay, nay!  Not so easy.  I had a heck of a time setting these
      states up.  After some long, grueling hours at it, all finally
      fell into place.  Ran several test runs successfully.

      Second problem occurred as the robot fix was concluding.  We
      took an electrical hit from a storm, knocking the systems out.
      Along with it went the DI water going off.  The system was
      rebooted immediately, but we had to wait 10-15 minutes for the
      water to come back on.

      						Doc
 
45.42robot finger position error SUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 08 1995 22:1015
SUBPAC::LANDRY                                       12 lines  29-JUL-1995 18:03
                        -< robot finger position error >-
--------------------------------------------------------------------------------
    
    	The robot finger position errored today.  See a couple of notes
    back for Fridays Robot Finger Positioning happenings.  Anyway, the 
    systyem cvouldn't recover due to the robot not recognizing it's
    position.  I attempted to manually move the robot around to recover the
    wafer, but it didn't go well.  The wafer broke in the spin station.
    I cleaned up the five or six pieces it broke into (easy cleran) and
    then rtebootyed the system.  Ther robot worked well.  Assured the the
    flags were being made, which they were.
    
    							Doc
      
45.43PROCESS ENGINEERING ADJUSTMENTS CHANGEDSUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 08 1995 22:1013
SUBPAC::LANDRY                                       10 lines   4-AUG-1995 19:24
                   -< major adjustments made per / Pro Eng >-
--------------------------------------------------------------------------------
    After doing several expirements on A2 this morning, Frank Krupa asked
    that the megasonics arm height be adjusted to ~3/8", along with the
    adjusting of the generator to the max setting.  We also adjusted the
    megasonics flow rate meter to 500 ML (a setting of 5 on the flow
    meter).  These changes will improve the particle removement perform-
    ance dramatically.  Other changes will follow as the operations spec
    needs to be DCO'd first.
    
    						Roger  /  Doctor
    
45.44carriage problems SUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 08 1995 22:1135
ASDG::POIRIER                                        11 lines  16-AUG-1995 20:09
              -< SPin Station Back Plate Bracket Screws Stripped >-
--------------------------------------------------------------------------------
    
    * Spin Station alignment problem:
    
      Found the (back plate drive bracket) screws loose. We tried to
      tighten them but they were stripped. The two 8-32 screw holes were
      drilled-out and retapped to 10-32. The assembly was then reinstalled
      and adjusted. The plexiglass cover needs to be mounted and a
      verification run started. 
    
                                                                     John.
    

          <<< ASDG::DISK$SYS_DATA:[NOTES$LIBRARY]FILMS_ONLY.NOTE;1 >>>
                                -< Films Only! >-
================================================================================
Note 65.130                       CMP-SCRUB.A1                        130 of 145
SUBPAC::BJUBINVILLE "NFD Fire - Rescue"              13 lines  16-AUG-1995 08:37
                    -< Contamination and carriage problems >-
--------------------------------------------------------------------------------
    
        Contamination source suspected from CMP.A1 brought skid
     marks to the top brush in both stations.  Both brushes were
     changed and the passed MQC's.  
    
        Later this morning, the spin station grippers were not
     fully grabbing the wafers.  It was discovered that the carriage
     was tilted and had loose screws.  Once they were tightened, the
     tilt got worse.  After about an hour a screw had come lodged inside
     the hole and needed TLC to get it out.  1st shift has taken over
     and are looking into the fix now.
    
                                                 Bob and BJ
45.45spin and robot alignments, brushes replaced SUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 08 1995 22:1119
SUBPAC::BJUBINVILLE "NFD Fire - Rescue"              16 lines  16-AUG-1995 23:21
                -< spin and robot alignments, brushes replaced >-
--------------------------------------------------------------------------------

     
        The problem with the spin station was discovered by 1st shift.
     The 10/32 screws that were used needed to be shorter so 1/2" screws
     were installed.  The spin station and carriage alignments are now ok.
     The spin lock positioning was out 90 degrees.  The spin station shaft
     needed to be loosened up and repositioned.  The robot was now out of 
     alignment so I went through part of the procedure with Roger.  The
     robot now picks up the wafers ok.  
    
        The bottom brushes were replaced per ENG.  All (8) lower bearings
     were replaced as well due to stalling.  Wafers are being run now for
     VERIFY and brush break-in and we've expericenced no problems at all.
     The next reply will list all new current machine offsets.
    
                                                        Roger and BJ
45.46SYSTEM OFFSETS AS OFF 8/16SUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 08 1995 22:1214
SUBPAC::BJUBINVILLE "NFD Fire - Rescue"              11 lines  16-AUG-1995 23:22
                            -< new system offsets >-
--------------------------------------------------------------------------------
    
    The current System Offset settings are:
    
    Load Station______1310		Rotation @ Spin Station______871
    Unload Station_____490		Rotation @ Receive Sta._____1813
    Wrist @ Spin Sta___110 		Balde______________________11500
    Wrist @ Receive____240		Robot Fingers________________340
    Spin Xport Delay____40
                                                                       
    
    
45.47PROBLEMS WITH BRUSH HEIGHTS, EXHAUST AND NO AMMONIASUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 08 1995 22:1327
SUBPAC::LANDRY                                       24 lines  23-AUG-1995 19:18
                       -< some training / findings info >-
--------------------------------------------------------------------------------
                                
WED - 08/23/95
Ron Simmons from Ontrak worked on CMP-SCRUB.A1 today.  John Poirier, Doc,
and Brendan Finn, and myself were trained by Ron to perform the following:
	1 brush change procedure: NOTE: NEED A BUCKET IN CMP ROOM TO SUBMERSE
					THE BRUSH CORE IN TO MAKE INSTALLATION
					EASIER.
	2 brush parallelism: WERE OUT 
	3 brush height set-up: BOTH BRUSHES WERE SET TOO HIGH

In addition Ron performed a "once-over" on the tool and identified the
following issues; some of which were corrected:
	- No NH4OH was flowing to SCRUB.A1.  All flow regulators were closed.
	  even when they were opened, there was no supply and NO ALARMS!
	  Doc called Ashland chemical.  Shortly after the call we heard the low
	  flow alarm go off.  Soon after the NH4OH began to flow.  Plan to
	  look into this further tomorrow to determine how long this was this
	  way and why we had no alarms.
	- The exhaust for the spin station and brush stations are not set-up
	  correctly(their required exhaust tags are actually reversed).
  	  Brush station should be ~5 scfm.  Spin station should be ~50scfm.
	  Actual was ~16 scfm for both.

				Frank, Ron, Doc, John, Brendan
45.48BRUSH ROLLER ARM NOT OPENING, BROKESUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 08 1995 22:1315
SUBPAC::LANDRY                                       12 lines   2-SEP-1995 19:38
                        -< Broke it's arm.......ouch! >-
--------------------------------------------------------------------------------
    The system wouldn't release the wafer from the Outside Brush station
    today.  The left roller arm was broken.  The shaft would actuate, but
    the arm stayed stationary.  Replaced the arm tested several times.
    Back up and running.
    
    Just a reminder.........the bolts that hold the arms to the shaft
    should never be tightened to capacity.  Over tightening will only 
    stress the material.  Proper installation will leave a small gap at
    the slit on the locking flange.  No gap......No good.
    
    							Doc
    
45.49LEAKS IN THE BRUSH STATION TUBSSUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 08 1995 22:1414
SUBPAC::BJUBINVILLE "NFD Fire - Rescue"              11 lines   8-SEP-1995 07:13
                              -< Resealing time >-
--------------------------------------------------------------------------------
    
    
        Removed both outside brush station roller drive asmbly. 
      and re-siliconed the fitting.  It will be ok to use around 
      11:30am or so.   The brushes are in the DI sink cascading.  
      The one with the green strap through it is the TOP brush.    
    
          The other two shafts in the inside station were siliconed
     on the outside as well.
                                                   D shift
    
45.50brush station roller arm brokeSUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 08 1995 22:1411
PATE::GEE                                             8 lines  20-SEP-1995 00:58
                      -< Inside brush station roller arm >-
--------------------------------------------------------------------------------
    Problem : A wafer went past the inside brush station and stopped 
    	      before the spin station.
    
    	      We found the left inside brush station roller arm broken
    	      at the shaft. Replaced the arm and ran verification wafers,
    	      all set.
    
    					B shift
45.51Robot finger flags looseSUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 08 1995 22:1411
SUBPAC::BJUBINVILLE "NFD Fire - Rescue"               8 lines  27-OCT-1995 06:51
                         -< Robot finger flags loose >-
--------------------------------------------------------------------------------
    
    
         The system kept alarming for fingers not closed.  Upon
      removing the covers to the robot, we observed the flags
      were loose and needed tightening.  The entire robot open/close
      and wafer pick-up needed to be re-taught.
    
                                                  D shift
45.61wafer shattered in sendLUDWIG::RIDLONEliminate the obviousTue Dec 12 1995 06:4810
    Wafer shattered in send portion of machine (product). There was only 
    one wafer left in the cassette when it happened. Tried to duplicate
    problem by cross slotting a wafer but once the wafer reached the wafer
    sense the boat lifted off its sensor and the elevator returned to home. 
    The only thing we can figure for a reason is that the wafer was chipped
    or had stress cracks prior. Unit was cleaned and a cassette of dummies
    ran through with no problems. The subsequent particle check passed.
    
    
    					B shift
45.62Scrubber NH4oH OCP's Jumped-outASDG::POIRIERFri Dec 15 1995 19:3416
                                               
    
    * NH40H OCP Failure:
      -----------------
      The OCP failed at lunch time today stopping the flow of NH40H.
      Ashland cannot find the problem. They are currently working with
      Systems Chemistry to find a solution. In the mean time, we have
      continued running both scrubbers with the OCP connection in the
      OnTrak electrical cabinet JUMPED-OUT. The OnTraks cannot detect
      any drop in NH40H under the current circumstances. Therefore,
      the NH40H pressure must be visually checked before each production
      run.
    
      Please show all operators on your respective shifts the location of
      the Nh40H gage and instruct them how to read it.
    
45.63flukeLUDWIG::RIDLONEliminate the obviousSun Dec 17 1995 03:4614
    System alarmed for robot fingers not closing. Wafer was there fingers
    were closed but the flag wasn't being satisfied. The fingers were loose
    so I opened and closed them a couple of times but still it wouldn't see
    the closed flag. Went in to teach mode and increased the robot fingers
    from 190 to 200 which closed them tighter and satisfied the sensor.
    Opened and closed the fingers and everything was working but the
    fingers seemed to be closing too tightly on to the wafer. Put the robot
    fingers number back to 190. Opened and closed them and the play was
    gone that was noticed before I changed the numbers in the first place
    and the closed sensor was being satisfied. Tried it a couple of more
    times in manual with the same results. Resumed operation and it
    finished the lot with out alarming.
    
    					B shift
45.64feedback adjustment made to roller motorSUBPAC::LANDRYSun Dec 17 1995 19:088
    
    The system alarmed several times today for "inside brush station roller
    motor out of spec".  The system never stopped running, just alarmed.
    The rotation speed was checked with the tachometer.  It was spinning at
    41 RPM but the readout said 32-34.  So adjusted the board potentiometer
    for the readout to match the actual.  All is well!
    
    							Doctor
45.65Inside Brush Station rollersFABSIX::R_GEETue Dec 19 1995 07:0316
	* Inside brush station rollers not turning.

	 - Found DI water dripping down onto the motor shaft.

		Replaced the o-ring seal on the roller shaft.
		
		Installed an o-ring on top of the teflon o-ring
		housing to prevent the assembly from working up.
  
		Replaced the motor.

		Replace the motor driver board, it failed also.

		Calibrated the spin speed, allset.

					B shift 
45.66SYSTEM OFFSETS AS OF 12/21/95SUBPAC::BJUBINVILLENFD Fire - RescueThu Dec 21 1995 00:3619
    
               LOAD STATION               --  1310
   
               WRIST AT SPIN STATION      --  124
       
               WRIST AT RECEIVE           --  240

               SPIN XPORT DELAY           --  35

               ROTATION AT SPIN STATION   --  873

               ROTATION AT RECEIVE        --  1813

               ROBOT FINGERS              --  190

               UNLOAD STATION             --  490

               BLADE LIFTER               --  11250
                                             
45.67ROBOT ROTATION ADJUSTEDFABSIX::B_WESTPHALFri Dec 22 1995 17:1016
CMP-SCRUB.A1 - DOWN FOR NOT PICKING THE WAFERS RIGHT FROM THE SPIN STATION.
	FOUND THE ROBOT TO BE GRABBING THE WAFERS TO HIGH ON THE FINGERS.  THIS
	PORTION OF THE FINGER IS ALITTLE THICKER, PREVENTING THE ROBOT FROM 
	CLOSING PROPERLY GIVING A "FINGERS NOT CLOSED" ERROR.  ADJUSTED THE
	ROTATION FROM 873 TO 870, REBOOTED THE SYSTEM RAN A BOAT OF WAFERS W/
	NO FURTHER PROBLEMS.  TOOL WAS RETURNED TO PRODUCTION.  THE OFFSETS
        ARE NOW AS FOLLOWS:
                           ROT. AT SPIN     870
                           ROT AT RCV      1813
                           WRIST AT SPIN    124
                           WRIST AT RCV     240
                           ROBOT FINGER     190
                           LIFTER         11250
                           UNLOAD STATION   490
                           LOAD STATION    1310
45.68SYSTEM OFFSETS AS OF 12/22/95SUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 22 1995 20:4219
    
               LOAD STATION               --  1310
   
               WRIST AT SPIN STATION      --  124
       
               WRIST AT RECEIVE           --  240

               SPIN XPORT DELAY           --  35

               ROTATION AT SPIN STATION   --  870

               ROTATION AT RECEIVE        --  1813

               ROBOT FINGERS              --  190

               UNLOAD STATION             --  490

               BLADE LIFTER               --  11250
                                             
45.69Start-up for 12/29SUBPAC::BJUBINVILLENFD Fire - RescueFri Dec 29 1995 15:118
    
        The DI came on but is still out of spec so we didn't want
      to keep it to the tool so we shut off the DI feed and opened the
      by-pass.  Facilities still have some by-passes opened, that's
      why we don't have very high pressure.
    
     
                                                       Mitch,John,Leon,BJ
45.70CMP-SCRUB.A1 START-UP COMPLETESUBPAC::BJUBINVILLENFD Fire - RescueSun Dec 31 1995 14:3925
                CMP-SCRUB.A1 STARTUP CHECKSHEET
                -------------------------------

                                                       Shift       Date
                                                       -------     -------
  1.  Ensure that all necessary facilities are         B/C/D       12/31/95 
      available and ready to use.                      

  2.  Power up each system.                            B/C/D       12/31/95

  3.  Open incoming DI Water Valve to each             B/C/D       12/31/95
      system.                                          

  4.  Close UDR valve at each system.                  B/C/D       12/31/95

  5.  Replaced all PVA scrub brushes.                  B/C/D       12/31/95

  6.  Change RTC status to SCHEDULED DOWN and
      perform a Weekly PM on each system.              

  7.  Change RTC status to VERIFY and notify
      Operations that the systems are ready
      for MQC.                                       
                                                       
45.71AmmoniaFABSIX::R_GEETue Jan 02 1996 07:483
		* Ammonia was down from 8 pm to 3 am.

					B shift 
45.72multiple offset adjustments madeSUBPAC::LANDRYWed Jan 03 1996 17:5110
    The system faulted out this afternoon for "robot finger not closed".
    Upon checking out the problem, the fingers were overdriving closed.
    Began to adjust the offsets, when I noticed that the "robot at spin"
    position wasn't making it to the wafer.  So, adjusted the offsets for
    that, but found the "wrist at spin" position off.  Adjusted that
    offset, readjusted the fingers closed offset and tested system
    performance.  Voila!  Alls hummin' along well.
    
    							Doc
    
45.73Arm replacedSUBPAC::BJUBINVILLENFD Fire - RescueWed Jan 10 1996 06:204
    
        Replaced rear top roller arm in the outside brush station.
    
                                      BJ
45.74robot arm flag adjustmentSUBPAC::LANDRYWed Jan 17 1996 16:3514
    First thing this morning, the robot was failing to pickup the wafer
    from the spin station.  In fact, the fingers closed position was was
    a good inch away from wafer contact.  Upon check out of the system, 
    found that the open sensor was the actual culprit.  I hate to say it,
    but it appears that someone may have physically forced the arms open
    at some point.  Both flags were securely in-place, but the open flag
    was 45 degrees out of position.  Hhmmmm.....
    
    It took several attempts to set it up to where both flags would make
    during a normal cycle.  Then the robot closed position was re-taught to
    fine tune.
    
    					A Shift
                                                
45.75broken "exercise" wafer in spin stationSUBPAC::LANDRYSun Jan 21 1996 19:0714
    The system broke a wafer (of the exercise type, NOT product) in the
    Spin Station today.  It's unclear as to how it happened, as we don't
    normally monitor each wafer through it.  It most certainly wasn't
    the robot due to the fact that the spin station lock had not yet
    energized to secure the fingers in-place. It appears that the spin
    fingers didn't secure the wafer properly, and that the high speed (or
    dry cycle to some) sent it flying to it's death.  
    
    Anyway, the debris was removed, then vacuum'd, then wiped....rinsed..
    wiped and finally rinsed once more.  A cassette of wafers was run to
    verify system performance.   An MQC check was then performed and it 
    passed with excellent results.
    
    						A shift 
45.76Door latchSUBPAC::BJUBINVILLENFD Fire - RescueFri Feb 09 1996 05:166

     Tool kept alarming because the door latch alignment was out and
  couldn't latch.  Repositioned latch and monitored a boat of wafers
  without any problems.
                                        D shift
45.77OCP failureSUBPAC::LANDRYTue Feb 13 1996 19:349
Today, the OCP for the Ammonium Hydroxide kicked off, sending both
scrubbers into a halt mode.  Checked the pressure gauge and it had
40 PSI going to the machine.  So why did they alarm.  Well, the 
fault displayed a "timed out" (or something wordy like that).  We
weren't able to reset the OCP's.  Gave Ashland a call to check out
there end of the deal.  The computer that controls the OCP hichup'd.
They need to down load a couple of files and we were back in business.

      					Doc
45.782 X slotting???SUBPAC::LANDRYWed Feb 14 1996 19:2610
    Late in the shift, a wafer broke in the spin station.  The mess was
    cleaned up, exercise wafers were run and MQC's were performed.  The
    system is up.
    
    Now, as to why the wafer broke is a bit confusing.  I was shown a 
    cassette with double slotted wafers.  Not sure if was ingoing or
    outgoing cassette.  Anyway, exercise wafers ran like a champ.
    
    					Doc
    
45.79roller drive shaftSUBPAC::BJUBINVILLENFD Fire - RescueThu Feb 15 1996 06:279
    
          Water once again has plaqued our shafts.  This time it
      was the roller drive shaft in the inside brush station.  DI
      got by a defective o-ring and went down the shaft and freezing
      up the bearings.  The entire motor drive shaft needed to be 
      removed from the tool and cleaned.  After everything was cleaned
      up, the rollers ran smooth.

                                              D shift
45.80Contact phone numbers for OnTrakSUBPAC::TOOKERFri Feb 16 1996 10:5027
Here is the latest list of service contacts for OnTrak Systems.  These con-
tacts can be used to get answers to technical questions, field service requests,
and parts.


    1)  Ron Simmons:  Office - 508-643-2772
                      Pager  - 508-504-7906 (this is your best bet)

        If no response in one hour, contact area supervisor in Fishkill, NY.


    2)  Pat Paino (area supervisor), Fishkill, NY:

                      Pager - 800-963-5770

        If no response in one hour, contact area supervisor in Austin, TX.


    3)  Stan Jaskinski (area supervisor in Austin, TX:

                      Office - 512-448-4494
                      Pager  - 800-905-9275

    4)  Brad Clements (regional manager), Austin, TX: (best bet for nights)

                      Office - 512-448-4494
                      Pager  - 800-796-7363  PIN 193-3639 (7 X 24 response)
45.81IB Upper Brush Motor blues.....SUBPAC::LANDRYSun Mar 10 1996 18:5935
      Through most of the shift today, the system would occasionally
      alarm for an Inside Brush Station Upper Motor out of spec.
      The brush would spin as low as 85 RPM at times, other times
      it would spin within the 10% limits.

      Through indepth trouble shooting, it has been determined that
      the motor for that brush is the culprit to the problem.  WE
      calibrated the board for the motor driver and were unable to
      attain the proper spin speed.  The screen readout and the hand
      held tachometer coincided as low rotation (~ 85-95 RPM).  WE
      tried swapping motor driver boards with the outside brush station.
      The problem stayed with the IB station upper brush, AND the
      possible bad board was working fine for the outside brush station.
      WE also checked swapped bearings between the upper and low brushes
      with no change in where the problem still resided.  So, WE took
      a closer look at the motor.  By applying pressure to the electronic
      leads on the motor itself, we were able to change the rotation
      speed.  Again, proof that the motor is beginning to wimp out.  The
      leads are currently (no pun intended) positioned such that the motor
      is spinning at ~115-118 with the set point at 120 RPM.

      Of course storage cabinet VSR-1 in the stockroom is down.  We are
      unable to attain the motor from the cabinet (there are 3 in there).
      WE have placed a call to the local OnTrak contact (Ron Simmons)
      at his home here in lovely Massachusetts to see if he may have 
      a 30.3 VDC motor to lend us until we can get our hands on one.
      We hope to receive a return call from him.  He has been supplied
      my (the Doctor) beeper number as well as the fab phone number in
      his voice mail.

      By the way, an MQC check was performed to make sure that the slower
      rotation speed wasn't causing any problems.  MQC's were real good.

      						A Shift
45.82Inside brush station top brush motor.FABSIX::R_GEEMon Mar 11 1996 07:055
	The inside top brush station motor failed. Replaced the
	motor with one found in J.T.'s cabinet, we couldn't get
	one from stock. No errors after the motor was installed.
     
					B shift 
45.83Lower brushes hesitatingSUBPAC::BJUBINVILLENFD Fire - RescueThu Mar 14 1996 23:377

        Noticed during weekly PM that the lower brushes in
   both scrub stations were hesitating while rotating.  
   Replaced all (8) delrin glass ball bearing to fix.

                            BJ
45.84NH4OH drip manifold testsSUBPAC::KRUPAWed Mar 20 1996 17:4360
03/20/96	FJK & JT & Ron Simmons OnTrak

	Subject:  CMP Scrubber NH4OH drip manifold tests

Summary:
   Today we tested the drip manifolds to deliver NH4OH to CMP-SCRUB.A1 in
place of the current spray manifolds.  The benefit of the drip manifold is
a reduction of ~6X of NH4OH used compared to the spray manifold.  Today's
tests consisted primarily of performing MQCs and comparing to std particle
results.  Particles looked good with the drip manifolds.  The wafers will be
submitted for mobile ion contamination testing prior to releasing the drip
manifolds to production.

Experimental:
   MQCs were performed on CMP.B1 and wafers scrubbed on CMP-SCRUB.A1 using 
the standard SPRAY manifolds and recipe.  The SPRAY manifolds were then 
replaced with the DRIP manifolds.  Scrub only MQCs were performed to ensure no
mechanical problems were induced during install.  Then MQCs were performed 
again on CMP.B1 and wafers scrubbed on CMP-SCRUB.A1 using the DRIP manifolds 
and a modified recipe(10sec added to NH4OH step and 10sec removed from H2O
step).  Finally the DRIP manifolds were replaced with the SPRAY manifolds
pending the outcome of mobile ion contamination tests to compare the two types
of delivery manifolds.  The results of all tests are tabulated below.  


	CMP.B1+CMP-		CMP.B1+CMP-
	 SCRUB.A1 		 SCRUB.A1
	REMOVAL	%STD		REMOVAL	%STD	
HEAD	PER MIN	DEV		PER MIN	DEV	
----	-------	----		-------	----	
1	3495	12.1		3216	8.6	
2	3503	7.8		3166	4.0	
3	3226	6.4		2845	3.1	
5	3232	9.3		2902	6.4	


	CMP.B1+CMP-		CMP.B1+CMP-
	 SCRUB.A1 		 SCRUB.A1
	LARGE	TOTAL	        LARGE	TOTAL
HEAD	DEFECTS	DEFECTS		DEFECTS	DEFECTS	
----	-------	-------	        -------	------- 
1	124	557	        162	553 
2	103	357	        89	250
3	96	299	        197	852 
5	105	389		167	730  			



CMP-SCRUB.A1 ONLY:  LARGE DEFECTS = 1; TOTAL DEFECTS = 18


Note:  The fab was evacuated after the spray manifold test and prior to the 
drip manifold tests.  The pad on the polisher was not kept wet during this 
period(~1hr).  This may account for the lower removal rate and slightly higher
defectivity on the DRIP manifold wafers.  Also, the initial MQC was too center
fast, so we adjusted the ID from 97 to 100 and the OD from 133 to 130 prior to
the drip test and is the cause for the reduced uniformity.  Finally the defect
data reported is POST only data not DELTA.  The SCRUB only results are right 
in-line w/where the tool normally runs.

45.85Wafer breakSUBPAC::LANDRYWed Mar 27 1996 18:3414
The system broke a wafer this afternoon in the Send Station.
There wasn't any equipment problems that caused this.  It was
an unfortunate bit of luck with the Opts people.  The cassette
was mistakenly joggled, hence the cassette present switch state
changed which allowed the lead screw to begin resetting.  As 
fate would have it, a wafer was beginning to exit the cassette 
at this time.  Crash!!! The wafer was dirven into the upper 
section of the entrance mouth of the Outside Brush Station.

Thouroughly vacuum'd up the wafer fragments from the Send 
Station and Outside Brush Station.  Rinsed said station several 
times.  Ran several test wafers.  Ran MQC's.  All is well.

      			A Shift and special guest Hawk
45.86CMP-SCRUB.A1 shutdown completed for facilities tie-inSUBPAC::BJUBINVILLENFD Fire - RescueThu Mar 28 1996 06:1728

  SHUTDOWN: 5:00 AM ON 3/28/96
  STARTUP:  9:00 PM ON 3/28/96


                CMP-SCRUB.A1 SHUTDOWN CHECKSHEET
                --------------------------------

                                                        Tech.       Date
                                                       -------     -------

  1.  Change RTC status to SCHEDULED DOWN.               LEON      3/28/96
                            
  2.  Remove all PVA scrub brushes and submerge
      in DI water.  If possible, DO NOT remove
      the brushes from their cores.                      LEON      3/28/96

  3.  Perform a complete wipe down and dry of
      all wet surfaces.                                  LEON      3/28/96

  4.  Close main incoming DI Water valve to each
      system and open the DI Water return valve
      (UDR).  This will allow all incoming DI Water
      to flow to UDR.                                    LEON      3/28/96

  5.  Power down each system.                          
                                                         LEON      3/28/96
45.87water leakFABSIX::L_SHKOLNIKOVThu Mar 28 1996 07:028
    
	Inside brush station rear arm. Water coming through the motor shaft.
	Removed old motor and shaft and resealed water leak, and changed
        o-ring on white cap. Roller motor wasn't replaced - non of them
        in the stock room 6.

						D-shift                

45.88Inside roller assemblySUBPAC::BJUBINVILLENFD Fire - RescueFri Mar 29 1996 07:2318


         This tool never came up from the shut-down.
     The roller arms in the inside brush station wouldn't
     stay closed thus letting wafers roll right on 
     through.  The roller themselves were kept stopping.
     The entire roller motor shaft assemble is junk.
     I took it apart and broken bearings and washers 
     were everywhere.  The teflon bearing that connects
     the shaft to the motor was junk.  The main shaft
     has all kinds of wear marks and needs to be replaced.
     Not many of the parts were in stock and not enough
     to get things working again.  I will speak to Jim T.
     about getting this stuff rushed in....

                                                BJ

45.89The parts for cmp-scrub.a1 will be here Saturday, 3/30/96SUBPAC::TOOKERFri Mar 29 1996 15:058
CMP-SCRUB.A1 is currently down waiting for parts.  The parts have been ordered
and are scheduled to arrive on Saturday, 3/30/96.  I have requested That
Security receive the parts from Federal Express at the HLO3 Security desk.
John Poirier and Brad Westphal will be here to install the parts.  Please
call me at home on Saturday if there are any questions or problems.

Thanks,
Jim T.
45.90"Inside Brush Station" Shaft/Arm Assy ReplacedASDG::POIRIERFri Mar 29 1996 19:218
    
    INSIDE BRUSH STATION SHAFT/ARM ASSEMBLY:
    ---------------------------------------
    The Inside Brush Station Shaft/Arm Assembly has been removed
    from WL-Scrub.A1 in the Wet Lab and installed into CMP-Scrub.A1
    in CMP. CMP-Scrub.A1 is currently running verification wafers.
    We will WUP the system after another sucessful run of 25 wafers.
    This latest run will be completed at 7:25 p.m.
45.91inside brush station / wl_scrub.a1FABSIX::R_GEESun Mar 31 1996 08:095
	Completed the inside top brush station roller motor and
	shaft assembly alignments. Re-assembled WL_SCRUB.A1 
	and ran 25 wafers, all looks good.

					B shift 
45.92Arm replacedSUBPAC::BJUBINVILLENFD Fire - RescueWed Apr 03 1996 08:095
    
          Replaced broken lower front roller arm in the  
       outside brush station.
     
                                        D shift
45.93Shaft and o-rings replacedSUBPAC::BJUBINVILLENFD Fire - RescueTue Apr 09 1996 13:307
    
    
          Replaced front roller drive shaft and o-ring seal
      in the outside brush station.  we also replaced the 
      o-ring seal in the rear roller assembly in the same
      station.
                                      A shift + EE
45.94Wafer sensor and PIA board replacedSUBPAC::BJUBINVILLENFD Fire - RescueTue Apr 09 1996 19:567
    
         The inside brush station entry wafer sensor went 
      south.  It took out the PIA board for cable #1 and #2.  
      Replaced PIA board and sensor.  Ran wafers and everything
      was ok.
    
                                      A shift
45.95Spin Station / inside brush station rollersFABSIX::R_GEEWed Apr 10 1996 08:0715
	The system went down for outside roller arms not opening. 
	Found the bracket under the station that moves the arm assembly
	had loosened up, tightened the bracket.

	The spin station fingers were missing the wafers intermittently.
	Found the wafer was being positioned in the spin station off
	center. Adjusted the sensor offset to 35 and adjusted the wafer
	exit position out of the inside brush station more to the back
	of the system. This needed to be done to compensate for the drive 
	belt being stretched and needs to be run on the smaller groove. 
	This makes the wafer exit out of the station higher on the back 
	side and shoot the wafer slightly to the front of the system.
	The system will run fine like this until new belts can be ordered.
	 
						B shift 
45.96wafers not exiting outer stationFABSIX::B_FINNTue Apr 16 1996 20:079

	Wafers intermittently not leaving outer clean station. Arms moving
        out,  but not enough. 
        Adjusted outer station left roller to match inner station left roller 
        position. Ran wafers, tested aok.


      						A shift
45.97Motor speed errors, loose gearSUBPAC::BJUBINVILLENFD Fire - RescueWed Apr 17 1996 05:5710

         Tool kept alarming for outside roller motor speed
     out of spec and no turning as well.  Found the rear
     pulley that is mounted to shaft to have loosened up and
     rode up the shaft.  This caused the belt to bind up and
     cause the motor to stall.  Re-aligned pulley and tested
     ok....

                                       BJ
45.98Inside Brush station FABSIX::R_GEEMon Apr 22 1996 08:0912
	The system went down for the inside brush station roller
	speed out of spec.
	Found a water leak was dripping onto the motor that
	rotates the rollers, the motor was full of water. We 
	replaced the o-ring that is in the shaft cap and installed
	a second o-ring under the cap. Replaced the motor,  
	repositioned the motor, motor bracket and drive assembly so if
	there is ever another leak it won't take out the motor.    
	Also, there was a crack in the poly housing around the
	shaft feedthru, we put silicone around the outside of it.
 
						B shift 
45.99scheduled contractor work performedSUBPAC::LANDRYTue Apr 23 1996 19:5220
      Today...........

      The DI water input to the room was shut down to perform
      some scheduled work with the DI line AND the OCP's had
      work done concerning the communications/electronics
      package.  This necessitated us to remove ALL the scrub 
      brushes so that they may be placed in water to keep wet.  
      All brushes were labeled and re-installed in their original 
      station/position.

      Ashland performed some electronic/communication work on the
      OCP's.  They verified that the work done to assure proper
      communication between the delivery system/OCP/scrubber.

      Once the water came back on and the system were allowed to
      be started up again, the brushes were installed, test wafers
      were run through the system, and MQC checks were performed.
      The system came back up with no problems.

      						A Shift / Jim T 
45.100motor and board changeSTRATA::SWENSONFri May 03 1996 16:0315
     Problem 1:: Inside brush station top brush stopped rotating.
         Fix 1:: Replaced top brush motor. Calibrated D.C. Motor P.C.B.

     Problem 2:: Upon boot up lost Wafer Transport Motion.
         Fix 2:: Attempted to calibrate Wafer Transport P.C.B. and
                 found R31 to be non responsive. Swapped with known 
                 good transport board and found problem to move with 
                 original transport P.C.B.
                 Installed with new P.C.B. from stock and recalibrated.

                 Doc and Hawk



45.101double loading problemSUBPAC::LANDRYTue May 07 1996 20:3527
          Today..........

      	I was summoned to the system to investigate why the system
      was going into an alarm state.  The alarm was for "looking for
      Inside Brush Wafer" or something close to that.  Observed the
      system and found that the Outside Brush Station was releasing
      the wafer, allowing the wafer to slide atop the wafer in the
      Inside Brush Station.  When I say release, I mean that the entire
      station acted normally with the lifter, rollers, transport belt
      all working like it was the normal time to release the wafer.
      All this despite the IB station showing it's status as "IN PROCESS".
      This happened 3 or 4 times within an hours running.  This made
      absolutely no sense what-so-ever.  So, I checked all the boards
      and their respective connectors for any loose/crooked connections.
      I didn't find anything abnormal, although I did remove and reseat
      several connectors.

      Upon reboot, ran 60 wafers flawlessly.  Had to give it back to them
      as I couldn't reproduce the problem.

      ps.  Yes, I did try rebooting the system several times before looking
           at the electronics.  And yes, I did talk to the rep about the 
           outcome.  He's never experienced this problem, but felt the 
           reseating was probably the fix.

      						Doc

45.102Outside brrr station.FABSIX::L_SHKOLNIKOVThu May 09 1996 07:439
    
        *** Outside brush station - water leaks through the drive shaft
            of the rear arm. Bearing parts was found under the shaft
            assembly. Entire shaft assembly needs to be replaced.
            We do not have replacement parts in stock. I will speak to Jim T.
            about getting this parts rushed in....

                                                Leon.

45.103Motors offsetSTRATA::RIDLONEliminate the obviousMon May 13 1996 07:506
    The wafer rotation motors on the brush stations were relocated. Orings
    are being used in the interim until the belts, which have been ordered,
    arrive. The belt is the same used to raise and lower the indexer.
    
    		
    					B shift
45.104The new NH4OH drip manifolds have been installedSUBPAC::TOOKERTue May 14 1996 17:167
Today the new NH4OH drip manifolds were installed on the inside and outside
brush stations.  The new flow meters have not been installed.  If flow
adjustments are needed, adjust the flow meter until the NH4OH goes from
a fast drip to a steady stream.  After the manifolds were installed, monitors
were cycled to verify operation and MQC's were performed.

Jim
45.106New NH4OH drip manifolds have been installedSUBPAC::TOOKERTue May 14 1996 17:187
Today the new NH4OH drip manifolds were installed on the inside and outside
brush stations.  The new flow meters have not been installed.  If flow
adjustments are needed, adjust the flow meter until the NH4OH goes from
a fast drip to a steady stream.  After the manifolds were installed, monitors
were cycled to verify operation and MQC's were performed.

Jim
45.105broken motor couplingSTRATA::FINNTue May 14 1996 21:217
	System was put down at 7:20pm for  outside lower brush not rotating.
        Found the 3 prong motor coupling nipple broken off. Brian is attempting 
        to locate or borrow one.


						A shift
45.107Coupling broke/replacedSUBPAC::BJUBINVILLECMP-6 Equipment EngineeringWed May 15 1996 08:267
    
       
          The drive coupling for the lower brush in the outside
       brush station was found broke on A shift.  Leon pulled
       the part from stock and replaced it.
    
                                               BJ
45.108Inside brush station roller speedFABSIX::R_GEEMon May 20 1996 07:375
	The system errored for "Inside brush station roller speed
	out of spec." With a setting of 40 rpm it was only rotating
	at 32 rpm. We tached the roller speed and adjusted the dc 
	motor control board.	 
						B shift 
45.109Spin Station Slide Assembly Air Cyl ReplacedASDG::POIRIERFri May 24 1996 20:2010
    
    Spin Station Assembly hesitating during Z Axis travel:
    -----------------------------------------------------
    
    The Spin Station Assembly was moving in a slow "jerking" fashion 
    as it moved from the Middle to the Bottom position.
    
    We replaced the 3 position Air Cylinder on the Spin Station 
    Slide Assembly. A 25 wafer verification run was performed with
    no further problems.
45.110No top rinseSTRATA::RIDLONEliminate the obviousMon May 27 1996 07:294
    Noticed that the spin station top rinse wasn't coming on during
    process. Isolated to faulty sv26. Replaced and tested fine.
    
    				B shift
45.111New brush heights / cylinder liftSUBPAC::LANDRYTue May 28 1996 20:2823
    
      Today, we started the system up from a shutdown situation.  At this
      time, new brushes were installed.  The wafer count was zero'd out
      in conjunction with the new brush install.  MQC's passed on the 1st
      pass.

      The New Brush Heights are:  IB-front 257      IB-rear 328
                                  OB-front 315      OB-rear 350

      The new brush heights have been  entered into the latest Weekly PM
      checksheet.  The Weekly PM has been performed for this week.

      The system is currently experiencing some difficulties with the Spin
      Station lift cylinder.  It occassionally alarms looking for the top
      position sensor.  Whats happening is that the spindle is remaining 
      at the bottom of the spin station, then comes up after a short pause.
      This is inconsistant in that it happened 4-5 times over the course of
      the day.  It will need to be looked at.
    
    						A shift
    
      						A shift
45.112Spin station lift assemblySUBPAC::BJUBINVILLECMP-6 Equipment EngineeringWed May 29 1996 07:3315
        Came into the shift with problems with the  spindle
      not always arriving to the top position and was alarming.
      It was intermitting all morning but since there was tons
      of work in the area, it was tolerable.  Around 3am it was
      failing after every wafer.  I increased the top solenoid
      air and backed off on the bottom solenoid air.  After 50 
      wafers and no problems, it was turned of to OPS.

        During this fix, a wafer had slid by the outside brush station
      rollers.  The front top roller arm was broke and needed to
      replaced.  That was taken care of.
    

                                             BJ
45.113Outside Brush Station Motor & Bearings ReplacedASDG::POIRIERThu May 30 1996 20:4111
    
    Brush Bearings:
    --------------
    The Outside Brush Station Brush bearings were replaced on both the
    top and bottom brushes.
    
    
    Brush Station Motor:
    -------------------
    The Outside Brush Station (Lower Brush) Motor was replaced and
    calibrated this afternoon.
45.114I.B. drive shaft replacement.FABSIX::L_SHKOLNIKOVSat Jun 15 1996 07:259
        INSIDE BRUSH STATION SHAFT assembly        
       ------------------------------------
    The Inside Brush Station Front Drive Shaft Assembly has been
    removed from the tool and replaced with a new one. I also replaced
    the o-ring seal inside of the white cap and checked roller 
    alignments. Scrub. A1 is currently running verification
    wafers.
                                           
                                                Leon
45.115carriage level adjustmentSUBPAC::LANDRYMon Jun 17 1996 20:548
    The system alarmed a couple of times today for "lost or broken wafer in
    the spin station".  The spin fingers were missing the wafer at the back
    grippers.....occasionally.  Found the carriage to be angled slightly to
    the front, hence angling the wafer to cause this mishap to happen. 
    Made a slight adjustment to level the carriage.  No failures
    re-occurred.
    
    					A
45.116heat lamp replaced.......SUBPAC::LANDRYTue Jun 18 1996 19:4116
      The Spin Station heat lamp burn't out today.  Thye filament was
      shattered into many pieces, not just a filament break.  Ordered
      a lamp from the stockroom, which showed an inventory of two spares
      lamps.  When attempting to pick up the lamp, the stockroom folks
      said that there were no lamps available.  Blah blah blah, blah blah.
      So, they said they would rush in a lamp, due to arrive tomorrow 
      morning.  In the mean time, we were granted permission to "procure"
      the lamp that belongs to A3, which isn't hooked up yet.  It was
      installed, but a test run failed.  The lamp wasn't firing up.  The
      problem was traced back to the 10A fuse, located in the electronics 
      cabinet.  Replaced the blown fuse and re-tested.  All is well.

      When the new lamp comes in, it needs to be placed on A3.

      						A
45.117Brush station rollersFABSIX::R_GEEWed Jun 19 1996 04:569
	The system was intermittently double slotting wafers at the
	inside brush station.

	Adjusted the outside brush station rollers up, so the wafer
	hits them in the center. 
	Adjusted both the inside and outside brush station roller arms
	in, so the wafers stop centered. 
	MQC's passed.
					B shift 
45.118Roller shaft replacedSUBPAC::BJUBINVILLECMP-6 Equipment EngineeringSat Jun 22 1996 08:1410
    
        INSIDE BRUSH STATION SHAFT assembly        
       ------------------------------------
    The Inside Brush station rear drive shaft assembly has been
    removed from the tool and replaced with a new one. I also replaced
    the o-ring seal inside under the white cap and checked roller 
    alignments. Scrub.A1 is currently running verification
    wafers.
                                           
                                                Leon
45.119spin to top adjustedLUDWIG::RIDLONEliminate the obviousSun Jun 23 1996 06:5014
    Alarming for "Timeout waiting for spin station at top sensor." Found
    that the spin shaft would eventually make it to the top. Adjusted the
    top, middle, and bottom solenoids and was able to correct the problem. 
    NOTE: Just an fyi, the solenoids for the spin shaft are labeled for the
    direction they send the shaft not to where they are connected to the
    bimba, ie., SPIN TOP sends the sation up which means its, obviously
    connected to the bottom of the shaft. Another Fyi, for the TOP and
    MIDDLE solenoids the bottom adjustment screws adjust the release of the
    air from the bimba while the top screws adjust the application of air to
    the bimba. The BOTTOM solenoid is the opposite. Clear as mud...right?
    
    
    					B-shift
    
45.120spin shaft solenoidsLUDWIG::RIDLONEliminate the obviousSun Jun 23 1996 22:327
    I was wrong....about the spin shaft solenoids.  
    The solenoids (and if you know this already good. I'm basically putting
    this in here for my sake) have two different outputs; A and B. The top
    screw adjusts the amount of air going to port A and the bottom screw
    adjusts the amount of air going to port B. The "SPIN TOP" and "SPIN
    MIDDLE" use port A and "SPIN BOTTOM" uses port B. 
    
45.121panel / gauges installedSUBPAC::LANDRYTue Jun 25 1996 20:4117
      While the room was shut down for a couple of hours today, we
      took advantage of that time and installed two inline gauges.  
      One for the DI Water and the other for Ammonia.  The gauges
      are mounted above the drip pan to the rear of the machine.
      It is necessary to remove the rear panel (on the Send Station
      end) to see the gauges.  These are currently only for convien-
      ience as they tie into a bigger project, which is alarm warnings
      at the touch screen, which we don't presently have the capability
      of on the systems today.  New software and boards will be installed 
      in the near future which will give us that capability.

      So, the two new gauges have been plumbed in place and are reading
      the pressures.  Be aware that 2% ammonia is flowing to it's new 
      gauge.  The lines were checked for leaks, none were found.

      						A  /  Jim T 
45.122Roller shafts replacedSUBPAC::BJUBINVILLECMP-6 Equipment EngineeringThu Jun 27 1996 07:3213

           The front and rear roller shaft assemblies
       in the outside brush station were replaced along 
       with the o-rings at the white shroud.

           Upon disassembly, the rear lower arm was found
       cracked so it was replaced.
                             
           All of the roller shafts in CMP-SCRUB.A1 have been
       replaced.  CMP-SCRUB.A1 will commence next.
                    
                                        D shift
45.123particlesSTRATA::WESTPHALFri Jun 28 1996 09:308
SCRUB.1 - Down for failing MQCs for high particles.  All brushes were swapped
	  out as requested by engineering.  The brush heights now set at 
          OB front 315 OB rear 350 IB front 313 IB rear 383.  All stations were 
	  cleaned and rinsed w/ DI water.  The IB exit rinse was not operating
	  so an adjustment was made to the appropriate AO valve.  Particles 
	  came in at 7.  The tool was returned to production.

45.124OnTrak after hours supportSUBPAC::TOOKERFri Jun 28 1996 11:286
Here is a telephone number that can be used for contacting OnTrak Systems
field service and technical support after hours.  This number will connect
you to an answering service.  They will forward your message to the people
who are on call.  The number is:  1-888-ONTRAK1

Jim T.
45.125power up o.k.LUDWIG::SWENSONFri Jul 05 1996 20:392
    Tool powered up with no issues
    waiting for di water.
45.126one flow meter installed, one to goSUBPAC::LANDRYSun Jul 07 1996 20:2613
    While performing the Weekly PM today...............
    
    The Ammonia flow meter was changed out (a planned change) in the OB
    station.  This flow meter replacement is part of the previously started
    retro-fit of the ammonia drip manifolds.  The IB station still needs to
    be retro-fitted in the future.  Time will be scheduled.
    
    Also today, the Weekly PM was performed.  The splash guards for the top
    brushes (in both stations) were missing.  They were found and
    re-installed.  
    
    						Doc
    
45.127spin station carriageFABSIX::R_GEESun Jul 21 1996 08:098
	The system errored for "wafer not found in the spin station".
	The dummy wafer never made it to the spin station, it was stopped 
	between the inside brush station and the spin fingers. It looks
	like the carriage rollers never started. While trying to recover 
	the wafer it broke in the spin station.
	Cleaned the spin station and ran 25 wafers, no problems noticed.
	MQC's came out good.
					B shift 
45.128Spin Station up travelFABSIX::R_GEETue Jul 23 1996 07:524
	The system kept erroring for "spindle not arriving up".
	Adjusted the air solenoid for spindle top and middle.

					B shift 
45.129di leak found/repairedSUBPAC::LANDRYMon Jul 29 1996 19:5610
    Whilst performing the Weekly PM today.........
    
    A DI leak was repaired.  The leak, which has been un-identifiable for
    a few weeks, was located at the fitting on the OB station drip
    regulator.  The fitting was te-taped and re-installed.  No more water
    was forming in the drip pan.  Hopefully, this puts an end to the leak
    situation.
    
    						A shift
    
45.130Spin station lift errorsSUBPAC::BJUBINVILLECMP-6 Equipment EngineeringThu Aug 08 1996 07:5210
 
          The tool was down at shift change for the spin station
       not coming up when told.  Replaced "little giant" air 
       cylinder and ran 50 wafers without any problems.  The 
       scrubber ran fine for the rest of the morning without
       any problems.

           Quarterly PM completed
                                               BJ
45.131Ammonia leakFABSIX::R_GEESun Aug 11 1996 07:395
	A fitting behind the inside brush station ammonia flow 
	regulator was leaking. Removed the regulator and re-teflon 
	taped, all set.

					B shift 
45.132Do not use the rubber boots on the carriersSUBPAC::TOOKERFri Aug 16 1996 15:5912
Yesterday during Strasbaugh's visit, we learned that they no longer 
recommend using the rubber boots on the carriers.  Their data now
shows that the boot is interfering with the free movement of the
gyro bearings and therefore impacting uniformity.  The boot was
designed to keep slurry from getting into the gyro bearings.  Be-
cause the carriers are disassembled and cleaned every few hundred
wafers, not using the boot should not cause a problem.  I have
gone through the cmp and carrier build room and removed all of the
boots.

Thanks,
Jim Tooker
45.133IB station wafer rotation problemSUBPAC::LANDRYMon Aug 19 1996 20:308
    The system has an intermittant problem with wafer rotation in the
    Inside Brush Station.  Found a broken arm in the station.  This was
    replaced and the results tested.  It appears to be better, but not
    up to it's recommended performance.  Occassionally, a wafer
    "flinches" as it's attempting to rotate.  If someone gets the 
    opportunity tonight, please see what you can do with it.  
    
                                                        Doc
45.134CM-SCRUB.A1 SHUTDOWN CHECKSHEETFABSIX::R_POIRIERMon Sep 02 1996 02:5220
                CMP-SCRUB.A1/.A1/.A3/.C1-7 SHUTDOWN CHECKSHEET
                ----------------------------------------------

                                                        Tech.       Date
                                                       -------     -------
  1.  Close main incoming DI Water valve to each
      system and open the DI Water return valve
      (UDR).  This will allow all incoming DI Water
      to flow to UDR.                                  ___B___     _9/1/96_

  2.  Remove all PVA scrub brushes and submerge
      in DI water. Label each brush with the
      tool name.                                       ___B___     _9/1/96_
  3.  Perform a complete wipe down and dry of
      all wet surfaces.                                ___B___     _9/1/96_

  4.  Power down each system.                          ___B___     _9/1/96_

  5.  Enter checksheet into notesfile.                 ___B___     _9/1/96_
45.135NO TOUCH SCREEN CAPABILITIESSUBPAC::BJUBINVILLECMP-6 Equipment EngineeringThu Sep 19 1996 08:0123
    
          Tool down at shift change for no touch screen capabilities.
       The touch screen wouldn't let us go to the touch screen 
       calibration target.  Tried cycling the power several times
       without any luck.  Swapped the following out with C-7 tool:
       
                        video card and cables
                        interface w/cables
                        ribbon cable to RS232 bulkhead
                        monitor
    
                                     no luck....
    
              I spoke with Patrick from OnTrak office in New York
        and he we went the right way and surprised it wasn't one
        of them.  As a last shot, he had us swap out the CPU.  
        still didn't work.  He suspects corrupted software and/or
        the video driver issues.  He is sending a REP A.S.A.P. out
        of his office and someone will be here ~10:30am with laptop
        and software in hand.  Since Jim is out, he will contacting
        Tim. in the a.m. as well.
    
                                            D shift
45.136IS Brush Station Roller Arm / Transport Belt SlippingASDG::POIRIERThu Sep 19 1996 20:3210
    
    Roller Arm:
    ----------
    The Inside Brush Station Roller Arm was cracked. The Arm was replaced
    and adjusted. 
    
    The Inside Brush Station Transprt Belt appears to be slipping
    intermittently. D Shift is picking up the Belt issue.
    
                                                                 C shift.
45.137Brush stations went out.FABSIX::L_SHKOLNIKOVFri Sep 20 1996 08:3415
    
        Came into the shift with problems with the outside station lower
       brush had some hesitation as it rotated in idle speed and it would
       not send the wafers in inside station. To fix that we replaced all
       brushes bearings and both drive belts. Works fine now.

       Inside brush station. The wafers were not spinnig but wobbling.
       Found that the guide rollers were out of alignment and the set 
       screws which hold all shaft assembly in place were not tightened.
       WE tightened set screws and spent some time on rollers alignment.
       Run 75 verification wafers looks good. No alarms so far. Returned
       tool to production. Needs full MQC's. 
                          
                                                              D shift.
                                                                         
45.138Outside brush station problemsLUDWIG::WESTPHALSat Sep 21 1996 20:456
SCRUB1 - Down for a loud Squeak in the OB, OB upper motor errors and the wafer
	 riding over the top of the rollers in the OB station.  Found the
	 Squeak to be coming from the back roller took the shaft apart and 
	 cleaned and adjusted belt tension.  The roller heights and motor issue
	 still needs to be addressed.  Ran out of time. 

45.139motor/rollersLUDWIG::RIDLONEliminate the obviousSun Sep 22 1996 06:0511
    Replaced the motor and calibrated. Read D-shift's passdown about the
    rollers. We found the same problem. Rollers misaligned (the OB
    station's rollers weren't even aligned with each other) and screws not
    tightened. So who's adjusting these things without putting something in
    notes? Readjusted the rollers and tightened the screws (but not too
    tight, don't want to bust those fragile plastic arms). Ran some wafers
    through that looked good.
    
    
    						B-shift
    
45.140Update on pressure interlock upgradesSUBPAC::TOOKERWed Oct 02 1996 17:279
Today OnTrak field service continued the pressure interlock upgrade work on 
the scrubbers.  The work is complete on cmp-scrub.a3 except for tying into the
NH4OH supply.  The tie in will require all scrubbers to shutdown for 30 min.
The work on cmp-scrub.a1 is still ongoing.  The electrical work is complete,
but still have the plumbing left to do.  When OnTrak field service leaves today,
cmp-scrub.a1 will be available for Operations to run product.  Work will
continue tomorrow.

Jim
45.141UPGRADESTRATA::WESTPHALWed Oct 02 1996 20:566
SCRUB.A1 - Was at scheduled down today for upgarades.  Sensors are being
	   installed to monitor pressures and check for proper operation of the
	   heat lamp.  The Ontrack Rep. will return tomorrow to install
	   software and work on .A2.  Tool presently sets in an up status
	   needing only MQCs.

45.142Update on pressure interlock upgradesSUBPAC::TOOKERFri Oct 04 1996 17:0315
Today OnTrak field service continued work on the pressure interlock upgrades.
They have now completed all necessary work on cmp-scrub.a1/.a2/.a3 except
for the following open items:

  1) CMP-SCRUB.A1:  Needs new software installed to enable the new pressure
          &         interlocks.  The new software will arrive on Monday and
     CMP-SCRUB.A2   OnTrak will be back on Tuesday to install.

  2) CMP-SCRUB.A3:  Needs final connection of the NH4OH pressure interlock
                    to the incoming NH4OH supply line.  We will do this
                    ourselves because all three scrubbers will need to go
                    down for 45 minutes to perform this task.


    Jim
45.143broke a waferSTRATA::RIDLONEliminate the obliviousTue Oct 08 1996 06:267
    Dropped and broke a product a wafer. Found that the robot was too high
    over the lifter and the wafers were dropping into the blade. Increased
    the "robot at rcv" calibration by 5 counts. Observed several wafers
    unload and all looked good.
    
    
    						B-shift
45.144Alarms tied in / software changedSUBPAC::LANDRYTue Oct 08 1996 20:359
      New software was installed today.  The new software has allowed
      for the DI Water and Ammonia to be tied into the alarm package.
      Both fluids were tested to assure that the alarms worked when
      a lack of fluid pressure would occur.  The software also ties
      in the Heat lamp.  If the lamp fails to illuminate, the alarm
      sounds.  This featiures was tested as well.

      					A shift
45.145Ignore this alarmLUDWIG::WESTPHALThu Oct 10 1996 20:346
SCRUB.A1 - Both scrubbers have been alarming been alarming intermittently for a 
	  "leak detected in machine floor".  The rep believes the problem is 
	   being caused by a floating ground.  This does not effect the proper
	   operation of the tool.  If the error is received just clear and 
	   continue running.  ONTRAK is working on a fix. 
45.146OCP alarmFABSIX::B_FINNTue Oct 15 1996 15:416
	OCP alarm for NH4 no flow. Flow was good, tried to reset OCP,
        but could not, had to emo and reboot OCP controller


					A shift
45.147LOWER DI OUT OF SPEC ALARMSUBPAC::BJUBINVILLECMP-6 Equipment EngineeringThu Oct 17 1996 00:0210


          Tool keeps alarms for "low DI lower flow value."
        Incoming DI at 40psi and all DI manifolds flowing fine.
        Logged a WARNING on tool to ignore it at this time until
        E.E. can address a possible alarm setting tolerance that
        might need to be adjusted.
    
                                               BJ
45.148DI Water pressure switch setpoint loweredSUBPAC::TOOKERThu Oct 17 1996 15:568
To try to minimize the number of false alarms for low DI Water pressure we are currently seeing on cmp-scrub.a1, I
lowered the pressure switch setpoint to 15 psi.  The new software that Ontrak is working on will give us a time
delay before there is an alarm.  This time delay will allow for the normal pressure fluctuations that happen when
the solenoid valves are opening and closing without the false alarms for low pressure.  I will be removing the
warning from this tool.

Thanks,
Jim T.
45.149The expanded version.. :^)SUBPAC::BJUBINVILLECMP-6 Equipment EngineeringThu Oct 17 1996 20:1118
              <<< ASDG::DISK$SYS_DATA:[NOTES$LIBRARY]CMP.NOTE;1 >>>
                                    -< CMP >-
================================================================================
Note 36.148               CMP-SCRUB.A1 EE/PE PASSDOWNS                148 of 148
SUBPAC::TOOKER                                        8 lines  17-OCT-1996 14:56
                 -< DI Water pressure switch setpoint lowered >-
--------------------------------------------------------------------------------
To try to minimize the number of false alarms for low DI Water pressure we
are currently seeing on cmp-scrub.a1, I lowered the pressure switch 
setpoint to 15 psi.  The new software that Ontrak is working on will give us 
a time delay before there is an alarm.  This time delay will allow for the 
normal pressure fluctuations that happen when the solenoid valves are 
opening and closing without the false alarms for low pressure.  I will be 
removing the warning from this tool.

Thanks,
Jim T.
             
45.150Timeout Errors - Outside Brush StationASDG::POIRIERFri Oct 18 1996 20:2213
    
    * "Timeout at Outside Brush Station" Errors:
      -----------------------------------------
      The frequency of these errors has increased dramatically in the 
      last hour. It looks like the Send Station drive belt is not
      moving the wafer into the Outside Brush Station every cycle.
      A slight tilting of the cassette sends the wafer thru. All 3
      scrubbers are busy moving product at this time. Please adjust
      at the first available opportunity.
    
    
                                                           C Shift.
    
45.151BEARINGS SHOT IN SEND STATIONSUBPAC::BJUBINVILLECMP-6 Equipment EngineeringFri Oct 18 1996 22:4914

       Tool down at shift change for OUTSIDE BRUSH STATION TIMEOUT.
    Both pulley assemblies in the SEND station needed to have most
    of the bearings replaced and one shaft replaced.  The shaft 
    closest to the exit of the SEND station was and still is slightly   
    bent.  There was none in stock.  One will have to be ordered.
    The teflon bracket on the tower closest to the exit has a small
    hairline crack at the "fork" end at the front roller.  This will
    eventually need to be replaced as well.  Tool ran a boat of wafers
    with no problems.  Tool went over to OPS for MQC's.   
                                               

                                               D shift
45.152new brushes / height settingsSUBPAC::LANDRYMon Oct 21 1996 19:0811
	Hi all,

		Just a quick note to let you know that the brush height
	readings for cmp-scrub.a1 have changed.  The brushes were replaced
	this week per process engineerings request, hence the necessity to
	change the micrometer settings.  The new settings are:

		IB - F = 345		OB - F = 270
		     B = 345		     B = 310

				Thanks.... the A shifters
45.153Recieve Station Lifter Did Not RiseASDG::POIRIERSat Nov 02 1996 19:2311
    
    Lifter failure:
    --------------
    The recieve station lifter failed to rise into position twice 
    this afternoon. The tool was powered down and rebooted. The 
    problem did not return.
    
     
                                                            C Shift.
    
    
45.154Semi Annual Incomplete Checksheet Posted.ASDG::POIRIERThu Nov 07 1996 19:385
    Semi Annual Incomplete Checksheet Posted. There is one item remaining
    on the semi annual p.m. Clarification is needed on the Brush Rotation 
    RPM procedure. 
    
                                                               C Shift.
45.155Some shorted wires.FABSIX::L_SHKOLNIKOVFri Nov 15 1996 23:3210

There was a problem with the send station wafer sensor. Timeout 
looking for cassette was going forever. Two out of three wire
connectors which located outside of send station were shorted out
to the metal pedestal of the sender and connector itself was 
sitting in water. The connector pins were replaced with new.
Tool runs fine since then.

                                        Leon.
45.156Low Ammonia alarm problem solvedSUBPAC::LANDRYMon Nov 18 1996 19:197
After a couple of days of intermittent "low ammonia" alarms, Ashland
was able to find the fault.  They traced the problem to a stuck valve
within their control panel down stairs.  The problem was fixed before
10:00 AM, with no alarms happening the rest of the shift.  Hopefully,
it stays that way.

                                  A shift
45.157low ammoniaFABSIX::M_RIDLONEliminate the obliviousTue Nov 19 1996 21:038
    Tool alarmed for low ammonia pressure. Gauge indicating a pressure of
    around 20psi with occasional dips below the 18psi setpoint. Called
    ashland to investigate and they couldn't find anything wrong but said
    they did cycle between pumps which brought the pressure up to around 25
    psi. Question whats a normal pressure we should be seeing?
    
    
    						B-shift
45.158low ammonia FABSIX::M_RIDLONEliminate the obliviousWed Nov 20 1996 01:358
    Had a few instances of low ammonia pressure after Ashland left. The
    pressure would go to 20psi and the dip below the setpoint momentarily. 
    If 25psi is the normal pressure perhaps the low setpoint should be
    lowered to compensate for these momentary dips in pressure.
    
    
    					
    						B-shift
45.159Regulator tie-inSUBPAC::BJUBINVILLECMP-6 Equipment EngineeringFri Nov 22 1996 06:559


            Tool is in BGN_EXTERNAL for contactors to install
        a DI regulator.  The brushes are in the white containment
        unit on the back table by the sink.  All (4) brushes are 
        clearly marked.                                               

                                               D shift
45.160Wafer sensor in spin stationSUBPAC::BJUBINVILLECMP-6 Equipment EngineeringSat Nov 23 1996 01:357
         The tool was alarming for "timeout waiting for wafer in
     spin station."  The wafer was there but the system wasn't
     seeing it.  Found the wafer sensor amplifier wasn't set
     properly and needed to be tweaked. 

                                              BJ
45.161fiber myopiaFABSIX::M_RIDLONEliminate the obliviousWed Dec 04 1996 03:408
    Timeout waiting for wafer in spin station alarm again. Too many alarms
    with too many tweeks, something else must be wrong. Checked the fiber
    optic cable with a flash light and sure enough found that some of the
    fibers weren't transmitting light. Replaced cable and recalibrated
    amplifier.
    
    
						B-shift
45.162marine motors required.FABSIX::M_RIDLONEliminate the obliviousWed Dec 04 1996 03:536
     Inside brush lower roller alarming for out of spec low. Replaced the
    bearings but it still alarmed. Pulled the motor off and it was full of
    water. Replaced and recalibrated. 
    
    					
    						B-shift
45.163sonic doulbe troubleFABSIX::M_RIDLONEliminate the obliviousMon Dec 09 1996 07:0511
    Tool alarmed for Mega sonic low flow. Found sv28 not opening when
    enabled. Replaced and flow worked fine, however, the arm would not
    sweep correctly. In fact the sweep was quite erratic. Sometimes it
    would sweep to the center and return BUT not to home and then other
    times it would start to sweep and 5 seconds into it (arbitrary number)
    and then the flow would turn off and the arm would stop. Found that the
    PIA card for the Mega arm sweep function to be faulty. Replaced and
    recalibrated the sweep home sensor and it worked fine.
    
    
    						B-shift
45.164Arm Home ErrorFABSIX::J_SWENSONThu Dec 19 1996 19:1610
    Megasonic Arm Home Fault
    
    - Increased the gain on the Megasonic arm home amplifier
    
    - Ran 50 wafers, could not repeat error
    
    - Tool ran the shift with no errors
    
    
                                C-Shift
45.165Low Ammonia Alarms / Shut Off Valve StrippedASDG::POIRIERFri Jan 10 1997 19:1725
    
    Low Ammonia Alarms:
    ------------------
    The system errored repeatedly for "Low Ammonia" today. The new gage
    that is connected to the alarm was reading from 9 psi to 20 psi 
    during the alarm event. (The other two scrubbers were reading a steady
    40 psi on their respective alarm gages.)
    
    Ashland checked everything downstairs and it was AOK. We attempted to 
    replace the alarm gage but the teflon shut off valve was stripped.
    It may be stuck half way open, we have no way of knowing. The knob
    and shaft turns in the valve but the pressure does not change. The
    shaft turns indefinitely in both directions. The nearest shut 
    off valve for the Ammonia is in the pipe gallery.
    
    Jim Tooker wants the valve replaced during the next P.M. We reduced
    the Ammonia flow on both brush stations from a steady stream to a
    steady drip. This seems to have stopped the tool from repeatedly
    alarming for Ammonia Flow. The tool has been placed on WARNING until
    the shut off valve is replaced and the ammonia flow is increased.
    
                                                         C Shift.
    
    
    
45.166valve replacedFABSIX::M_RIDLONEliminate the obliviousMon Jan 13 1997 07:265
    Replaced the ammonia shut off valve during the weekly. The one removed
    was all the way open.
    
    						B-shift
    
45.167Meagsonics sweep errorsFABSIX::R_POIRIERSun Jan 19 1997 07:0811
	We had a problem with the Meagsonics sweep last nite.
	It would not home after a sweep. Tried adjusting the
	gain and it worked for a little while. Then error would
	come back. Found that the home sensor was to close to 
	the base plate. Adjusted sensor up off the plate and
	sweep worked fine the rest of the nite.


					B shift

45.168Status of new software rev.SUBPAC::TOOKERWed Jan 22 1997 15:398
    OnTrak field service came in today to install a new revision of
    software.  This new revision will add a small time delay before
    alarming for low DI Water or NH4OH pressure.  This will help to
    eliminate alarms due to pressure fluctuations from valves actuating.
    However after doing the installation, OnTrak found a bug in the
    software.  He removed the new rev. and re-installed the old rev.
    
    Jim T.
45.169Possible cure to high particlesSUBPAC::LANDRYTue Jan 28 1997 19:2412
Whilst checking the system today, it was noticed that the megasonics sweep
arm was not sweeping to it's proper dimensions.  The actual sweep distance 
was fine, as that motor is rotating fine.  The air cylinder, which positions 
the megasonics arm at the edge of the wafer prior to the sweep motor turning
on, was found to be mechanically wedged.  This was caused by the backing out
of a threaded rod (which is used to make the connection with the pivoting
portion of the assembly).  Re-threaded the rod into the block.  Re-attached 
pancake valve and associated bracketing.  Tested and achieved positive results.
We'll monitor the system occassionally to assure that the rod stays in place.

                                           A shift

45.170lower brush bearings installedFABSIX::J_SADINFreedom isn&#039;t free.Mon Mar 17 1997 19:349
    
    
    	Replaced outside-station lower brush bearings today due to lower
    brush intermittently stalling. Running ok now.
    
    
    a-shift
    
     
45.171Particles....SUBPAC::BJUBINVILLECMP Equipment EngineeringFri Mar 21 1997 08:3827
    
         The tool seemed to be trending on the high side 
      for particles on the MQC's for the last two months. 
      First off, the megasonic unit was turned off.  
      All of the handling and alignments were checked and 
      seemed to be ok.  MQC's were run and the tool is 
      putting on 50 adders.  The bottom brush motor was 
      intermittently stalling and would sometimes stop.
      It could be started again by simply touching the 
      motor.  We pulled the motor and found all kinds of 
      carbon build-up within the drive shaft and coming 
      out of the motor as well.  The motor and bearings 
      were replaced and the area cleaned up.  There some 
      fine particles embedded in both brushes so were 
      ended up replacing all (4) brushes.  After 50 wafers
      were run, an MQC was run and it was slightly out
      of spec so I started up another 50 wafers.  The tool
      started alarming for Timeout For Wafer In Outside Brush
      Station.  The transport assembly wasn't turning.  The 
      main drive belt for that transport was replaced and
      got things running again.  We are running 50 wafers 
      now and we'll be running MQC's when they are done. 
      We'll see then if we found the problem.  After 24 hrs.,
      the brush heights will have to be re-checked and maybe
      adjusted.

                                            D shift
45.172particlesFABSIX::J_SWENSONFri Mar 21 1997 19:5336
    
    
    PARTICLE PROBLEMS                            
    -----------------
    
    - tool was cleaned from send to recieve.
    
    - amonia was adjusted to proper flow
    
    - 100 wafers run through the tool
    
    - particles failed @ 102
    
    - replaced outside brushes
    
    - ran 50 wafers
    
    - particles failed @ 113
    
    - adjusted brush heights
    
    - left 310
    
    - right 300
    
    - ran particle check on scrub a3 @ 7
    
    - ran last check on A1 particles @ 52
    
      the particles are coming down another 50 wafers will need to be run
      then the particles should come in.
    
      will pass on to D- Shift
    
    
                                          C-Shift 
45.173Auto reply system never posted this from 3/22SUBPAC::BJUBINVILLECMP Equipment EngineeringFri Mar 28 1997 07:2234

             Took over from C shift for the particles issue.
         After 100 wafers were run, the tool still failed for 
         over 100 particles.  All of the motors were pulled out 
         of the mounting shafts and there was carbon built-up on 
         all of them except the one motor we replaced yesterday.  
         There was signs of rust emitting from the outside brush 
         station transport assembly so that was all rebuilt with 
         new parts.  Both roller arm shafts and many associated 
         worn parts were replaced.  The inside station was in 
         fair condition as far as wear is concerned but no problems 
         were found.  The megasonic arm at home needed to be 
         adjusted. When it came home, the arm was whacking up 
         against the front panel.  The spray nozzle was bumped to 
         the left side of the wafer and wasn't spraying in the 
         middle of the wafer.  200 wafers were run through the 
         tool and MQC's were run...  both wafers came in spec
         and removed particles.   pre-5-29-0 post-5-27-0
                                  pre-6-32-0 post-5-24-0

         The tool was turned over to OPS but please monitor the
         MQC readings for a while to see the results stay near
         zero.  The brush heights ad been changed since C shift
         so below are the new numbers.
                                   
                                            D shift

                                  OB      IB
                                 ----    ----
The new brush heights are: Front 340      345  
                           Rear  350      345


45.174Roller motor brush motor issuesSUBPAC::BJUBINVILLECMP Equipment EngineeringFri Mar 28 1997 08:4317
    

          Tool initially went down for wafers not rotating
        in the outside brush box.  Upon discovery, the front
        roller arm was out of alignment and is still being
        worked on by C shift.  While checking the alignments,
        the bottom roller was rotating whenever it felt like
        it.  It was spinning at erratic speeds when set to 
        118 RPM's and was slowly rotating when told to stop.
        A motor controller board was checked and we found the
        jumpers in the wrong spots.  The channel was set up a 
        a non-programmable control versus a programmable.  The 
        jumper settings for that channel were suppose to be 
        J2, J3 and J8, not J1, J3 and J8.  After the jumpers
        were set and board cal'ed, the bottom brush worked
        fine.
                                             D shift
45.175o-rings (again)FABSIX::J_SADINFreedom isn&#039;t free.Tue Apr 01 1997 20:388
    
    
    	replaced outside brush station roller o-ring (send side) and inside
    brush station roller o-ring (receive side). These were the large
    o-rings that connect to the pulley on the transport roller motor
    (wafers were not being inducted/sent). 
    
    a-shift
45.176Receiver/heat lampSUBPAC::BJUBINVILLECMP Equipment EngineeringFri Apr 04 1997 07:0012
       Tool alarmed for "robot waiting for receive station."  
     The boat/receiver never RESET and manually resetting 
     wouldn't work either.  The cassette present switch was
     ok as well.  Ok..  Ok..  get to the point...  I powered
     down the tool and I heard a "pop."  Nothing seemed wrong
     until I went to run some wafers and the tool alarmed for
     no heat lamp.  Guess what the pop was.  The lamp filament
     blew.  After the lamp was replaced...  we were good to go...


                                                       D shift
45.177Robot Dropped Wafer / Lifter Did Not Rise UpASDG::POIRIERThu Apr 10 1997 20:2811
    
    Recieve Station Lifter:
    ----------------------
    
    The robot dropped a wafer into the base of the tool due to the lifter
    not rising up. This event happened around 6:00 p.m. The problem hasn't
    reoccured since the reboot.
    
    
                                                           C Shift.
    
45.178Wafer dropped by robotFABSIX::R_POIRIERMon Apr 14 1997 08:4113


		Scrubber robot dropped a wafer after the
		spin cycle. We were able to recover and 
		continue. This happened 2-3 times thru
		the night. Due to problems with the other
		scrubbers we didn't have the time to try
		and figure out the root problem.


					B Shift

45.179 Needed a rebootFABSIX::B_WESTPHALThu Apr 17 1997 20:284
    
SCRUB.A1 - Down for the robot not picking a wafer from the spin station.  The
	tool just needed the receive station reset.

45.180WAFER CRASHEDFABSIX::B_WESTPHALThu Apr 24 1997 21:118
SCRUB.A1- Down for smashing a wafer in the spin station.  Cleaned up the crash
	  and wiped down the OB, spin, And unload stations.  Noticed the
	  wafers were stopping in the spins station to early preventing the 
	  spindle fingers from grabbing the wafer properly.  Repositioned the 
	  sensor and ran 20 wafers w/ no problems.  Particles came in at 26 so 
	  the tool was returned to production.

45.181Dummy wafer dropped in receive stationSUBPAC::BJUBINVILLECMP Equipment EngineeringSat May 10 1997 09:136
    
            Robot dropped a wafer in the receive station.  Checked
         lifter and robot handling and they were ok.  Verified ok
         with 25 wafers.
    
                                                BJ
45.182robot teach functions changedSUBPAC::LANDRYSun May 11 1997 18:3717
    We encountered some problems today with the robot not picking up the
    wafer properly from the spin station.  A wafer was placed in the
    station, and we diagnostically checked out the functionalities.  It
    was discovered that there were several mis-aligned positions.  First
    off, the "robot position at spin" was off.  The robot teach function
    number for the "rotation at spin" setting was changed from 875 to 882.
    This allowed the 3 robot grippers to align to all grab the wafer. 
    Further inspection showed that the grippers were grabbing the wafer,
    but there was a difference between the back grip and the two front
    grips of where the wafer was gripped.  We then adjusted the "wrist at
    spin" teach number to allow the grippers to be planar to the wafer.
    Also, to fine tune the station, the robot gripper close teach number
    was adjusted.  It ran the entire day without further problems.
    
                There is no "I" in...........  A team
                                                 ----
    
45.183Lifter issue....SUBPAC::BJUBINVILLECMP Equipment EngineeringWed May 14 1997 07:3033
    

          First off - the tool still has higher particles during
       MQC's.  This is an on-going issue and that's why we've
       been trying to get it.
        
          Last night we noticed that certain product wafers don't
       particularly like the outside brush station.  The rollers
       are trying to spin the wafers counter-clockwise (looking from 
       the front of the tool) but the brushes are forcing the wafers
       to go the other way.  This friction is causing wear on the 
       rollers and according the class I went to, this is a source
       of particles.  The workload was big this morning and CMP.A1
       is going down for the monthly so I won't get to it.

            Twice the tool dropped a wafer in the receive station.
       The blade lifter never even came close to being high enough
       to get the wafer.  Therefore when the robot fingers opened 
       and tilted, there goes your wafer.  I haven't seen any ASSIST
       for this tool for dropped wafers but I know of at least three
       occurrences within the last week between C and D shift alone.
       After the second wafer I noticed the lifter wasn't high enough
       and I tried STOPPING the tool but it was to late and the wafer
       fell.  It got a small scratch.  I went into maintenance to 
       manually run the lifter but it wouldn't move.  Then the screen
       froze.  I EMO'ed the tool but there was a wafer in the spin
       station.  The fingers had the wafer and the carriage was still
       out so the wafer became two.  I went through all of the lifter
       assembly and I couldn't find anything wrong.  25 wafers were
       run and there were no problems.  The tool ran perfect for the
       rest of the morning.

                                                   D shift 
45.184robot/recievestationFABSIX::J_SWENSONThu May 15 1997 20:379
    Recieve station/robot issue.
    
     tool locked up with wafer in spin station.
    
     reset tool and could not recreate error so returned back to
    production.
    
    
                                     C-Shift
45.185Send station rebuiltSUBPAC::BJUBINVILLECMP Equipment EngineeringFri May 16 1997 06:257
    
         Rebuilt entire send station with all new bearings,
     belts ect.  Found alot of rust, cooked bearings and drive
     belts 50% stretched out than a new one.  All alignments
     were checked and verified.  Tool passed MQC's at 23.
    
                                               D shift
45.186DROPPED A WAFERFABSIX::B_WESTPHALBradley BP#661 EXT# 6610Sat May 17 1997 20:495
CMP-SCRUB.A1 - Dropped a wafer in the receive station.  The station was reset
	 and 25 wafers ran w/ no problem so tool was returned to production
	 with an assist.

45.187MEGASONIC NOT AT HOME.FABSIX::B_WESTPHALBradley BP#661 EXT# 6610Wed May 28 1997 19:4410
    
CMP-SCRUB.A1 - Down for "Megasonic arm not at home" errors and adjustments to
	the receive station.  While the tool was erroring The Megasonic arm 
	stayed over the spinning wafer waiting to see the arm sweep at home.
	the sweep home sensor was adjusted and the tool ran fine.  When the 
	problem first started I thought the receive cassette needed to be
	reset.  When I reset the station and the lifter blade missed the wafer 
	while checking for the wafer.  This scratched it.  The unload station
	offset was adjusted to correct this situation.

45.188C shift passdown regarding particlesFABSIX::B_JUBINVILLEWed May 28 1997 22:1118
From:	ASDG::POIRIER      "FAB6 CMP EQUIPMENT TECHNICIAN. PAGER # 254 FUNCTION 1. TEL:6610,5804,4774,6609." 28-MAY-1997 19:29:29.78
To:	FABSIX::B_JUBINVILLE,FABSIX::L_SHKOLNIKOV
CC:	POIRIER
Subj:	passdown



   Brian & Leon,

   Here is the latest situation:

   CMP-SCRUB.A1 - DOWN/UNSCHEDULED: Failed MQC'S for particles.
   We were working in the spin station this afternoon and probably
   contaminated the spin area. The PIA board for the megasonic sweep
   motor was replaced.


                                                            C Shift. 
45.189particles.FABSIX::L_SHKOLNIKOVThu May 29 1997 08:2526

          Came in with tool down for particles.  After
      running 50 wafers, MQC's were run and the tool 
      failed for 250 particles.  Replaced brushes and
      replaced the (4) smaller style rollers with the
      original larger style roller.  Ran a modified
      brush break-in recipe and checked particles.  
      They came in at 115.  Another 50 wafers were 
      run and the particles came in at 110.  We
      elimnated the megasonics and rinse and we
      got the same results.  We tried eliminating 
      each brush station and got pretty much the same 
      results but the outside station seemed to be
      in question.
      
Here is the results we got:

          spin only     IB            OB     Stras.best
7-29-0   59-237-0     12-31-0      18-61-0   36-78-0
3-31-0   40-76 -0     23-61-0      26-88-0   30-91-0

 We ran regular mqc and it failed again. 4-20-0 and after mqc 82-155-0.

                                                       D shift

45.190Particles FABSIX::J_SWENSONThu May 29 1997 20:3128
    Particles                            
    ---------
    
    
                 - picked up from D-shift
    
                 - noticed spin station belt worn
     
                 - ran mqc wafer blocking spin staion belt
             
                 - came in spec with 33 adders
    
                 - replaced spinstation belt and wiped down entire
                   spin station upper and lower, also entire recieve
                   station.
     
                 - another mqc wafer and 0 adders were found
    
    -------------
                 - towards the end of the shift had a lifter problem
                   which ops noticed.
    
                 - reset recieve station and ran 50 verification wafers
    
                 - no problems found, returned tool back to production.
    
    
                                      C-Shift
45.191Bad boats.....SUBPAC::BJUBINVILLECMP Equipment EngineeringFri May 30 1997 07:5619
    

           Tool stopped with no errors.  The boat in the
        receive station was warped and the switch couldn't
        be made.  The boat was replaced and the wafer that
        was in the boat was put into the new boat after 
        the station was reset.  When the lifter was checking
        to see if there was a wafer present, it missed the 
        1st wafer and dragged past it.  The wafer seemed ok
        and the PPS remarked the lot.  The robot somehow 
        nailed the cassette and the finger flags got lost.
        The robot sensors needed to be tweaked.  The tool ran
        25 wafers with out any problems and the tool was
        brought back up.
                                             D shift
     
    This second boat was
        found to be warped as well.  Both hit the trash can.