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Conference asdg::cmp

Title:CMP
Notice:Welcome to the CMP notesfile
Moderator:FABSIX::B_TOWERLLE
Created:Tue Oct 31 1995
Last Modified:Fri Jun 06 1997
Last Successful Update:Fri Jun 06 1997
Number of topics:94
Total number of notes:6381

41.0. "CMP.D1-7 EE/PE PASSDOWNS" by SUBPAC::BJUBINVILLE (CMP-6 Equipment Engineering) Mon Dec 30 1996 14:41

    
    
        This topic is designated for the Equipment and Process 
      Engineering passdowns for CMP.D1-7.
T.RTitleUserPersonal
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41.1CMP.D1 SOURCE REPORTYIELD::TDYERTue Feb 18 1997 10:10123
+---------------------------+ TM
| d | i | g | i | t | a | l |   I N T E R O F F I C E   M E M O R A N D U M
+---------------------------+
| S e m i c o n d u c t o r |
+---------------------------+

	To: MaryAnn Piasecki			Date: February 18th, 1997
      	    					From: Timothy P. Dyer, Bob Gee
	    					Dept: CMP Engineering
						ENET: Yield::TDYER
	cc: Frank Krupa				DTN:  225-5072
	    Dan Oconnor
	    Dennis Goodwin
	    Linda Bioseneualt
	    Ellen Mager
           
  Subject:  CMP.D1-7 (Speedfam Auriga #65, 952731) SOURCE INSPECTION REPORT 
_______________________________________________________________________________

Summary:
  Tool 65 was in a better state of readiness than past CMP tools which Digital
 source inspected at Speedfam. We could not determine what accounted for the 
 improvements, whether it was due to some new organizational skills or if it 
 was solely due to the new improved Auriga platform. In either case it made 
 the source inspection run much smoother. On 2/12 we conducted the initial 
 inspection which included configuration verification and a 500 wafer marathon.
 We created a recipe with the following basic parameters and began the 500 
 wafer marathon.
				DF = 350lbs
				Slurry = 350,350ml of KoH/DI
				CrSpeed = 35
				TblSpeed = 35
                     2nd table: 80lbs touch down, 150lbs polish, 15 seconds.

 Several unexplained software errors were encounter and the marathon was 
 terminated. Tool 65 was running version 1.3.4 software when it errored. We
 meet with Speedfam Software Engineering to discuss the problems and possible 
 related bugs. The Software group had a new release as of 2/8/97, version 1.4.1
 which was created to address some of the false software errors. We requested 
 1.4.1 be installed on tool 65. On the second day, 2/13 we re-started the 500 
 wafer marathon with version 1.4.1. The 1st wafer loaded at 9:15am, all wafers
 ran with out error and completed at 3:45pm, 500w/6.5h = 77w/h WOW! The Auriga
 ran with no vibrations on either table with pressures in excess of 350lbs with
 DI water ONLY. Tool 65 was accepted and ready for shipping with a few open 
 issues listed below:
	
Configuration Issues:
	1.  2nd table conditioner not ready, still in design phase, will be a
	    retro-fit.
	2.  Requested CMP-V standard vacuum filter set up.
	3.  SECS-II not installed. Software not released.
	4.  N2 line and CDA lines crossed.
	5.  Slurry pump cabinet door latch broke, needs replacement.

Test and Calibration:
	1. Scrubber speed cal not done or documented.
	2. Pad conditioner EPRV not caled or documented.
	3. Vertical table run out not documented.
	4. Slurry pump cals not done or documented.

Software Issues:
	1.  No issue after 1.4.1 installation. There are however several 
	    items such as error recovery which is desirable and will be added 
	    a "which list".

Automation frame:
	1. Load and Unload flipper drip pans a draining into the load/unload 
	   module. I have requested the trays be angled towards the main frame
	   and requested the automation drain be plumbed to the main 3" drain.

Miscellaneous:
	1. Vacuum pump exhausting water vapors due to insufficient vacuum tank
	   blow down. I have requested a frequency increase in the blow down, 
	   however this is hard coded in the software and will require a rev 
	   change.
	2. Luxitron order scratched from PO. Digital will rely on Speedfam
	   Endpoint system. Speedfam requested to submit FORMAL timeline and
	   plans for Digital beta testing.

Process Issues:
	1. No process tested. We wanted to avoid contaminating the tool and 
	   there is Digital NO process developed yet for the Auriga

OTHER ISSUES AND ACCOMPLISHMENTS DURING THE VISIT AT SPEEDFAM:

o Met with the engineering design team. We brainstormed several concepts for 
  the second table conditioner. We have agreed on a primary concept and a
  back-up concept. Engineering drawings will be create on the first concept
  and submitted for my review in a couple of weeks. The project time line for
  installation looks like late July early August.

o Met with the documentation department and discussed there plans and our needs
  for electronic documentation. They are planning on going with an HTML 
  format, the package will run very similar to a web browser and may require
  NetScape.

o Met with the Vise President of Sales and marketing and the Eastern sales 
  manager to discuss CMP.B1 reliability and plans and terms for an upgrade.

o Met with an Electrical Engineer from the reliability group. We discussed the 
  Infranor/motor project. They have corrected several problems related to
  failing infranor and motor stalls. There was NO algorithm in the infranor for 
  the specific motors onboard the CMP-V polisher. The infranor amplifiers were
  using the "closest matching program". They have sign loaded the amplifiers
  with the correct algorithm. This new program re-aligned the phase, which were
  previously 30 degrees out of phase and has the correct ramp and run rates
  programmed. The amplifier auxiliary power was dropped down from 205 to 115vac
  and the have installed more reliable filter capacitors. These changes have 
  power and efficiencies by 30-40%. Dynamic current monitor has decreased from
  4vdc to .5vdc, IRM has been lowered from 14.5vdc to 10.5vdc. A CMP-V polisher
  was tested at 450 of down force at Speedfam with NO stalling or high current
  draw issues. This will be implemented on CMP.B1,2,3,4 and should address the
  stalling problem.

o Meet with Bill Spencer, Carrier Films Manager. I have requested him to
  email me with a monthly carrier film service report. We will use this to
  do our blanket releases.
                
o Meet with Mike Slepekes, training manager, to discuss plan for Auriga
  training. I have scheduled an onsite training class immediately following the
  equipment start up of CMP.D1. One technician from B,C,D and myself will 
  attend.
41.2CONDITIONER REMOVEDYIELD::TDYERWed Feb 26 1997 15:356
    
     Removed conditioner end effector and bearing assembly. A custom
    conditioner will be installed in ~three weeks.
    
    TD
    
41.3FLUIDS CAB MODYIELD::TDYERThu Mar 13 1997 16:049
    
    The fluids cabinet MAIN DI line has been modified. The main DI line now
    enter the right top of the fluids cabinet passes across the valve bank
    than is routed (via a 90) down to the bottom of the valve manifold
    block. This was done to allow for room for the 2 slurry manifolds.
    
    fyi,
    
    TD 
41.4Vacuum pump / N2 pressure sensor linesFABSIX::R_GEEWed Mar 26 1997 18:588
      - Mounted the vacuum pump under the floor, it should be all set
	for now. We still need to put a second vacuum gauge in-line
	next to the filter housing.

      - Re-routed the N2 wires up to the new N2 pressure sensor location.

					A shift
	
41.5check outSUBPAC::CMPThu Mar 27 1997 19:112
    power up and checked a few functions. Tool seems to be ready for the
    installation next week.
41.6MAIN DISCONNECT LOCATIONYIELD::TDYERFri Apr 04 1997 14:226
    
    THE MAIN DISCONNECT FOR CMP.D1 IS IN THE SUBFAB. 6.2N. IT IS
    LOCATED IN THE CEILING ABOVE OXDEP.D2'S PUMP PACKAGE.
    
    FYI,
    TIM
41.7ConditionerFABSIX::R_GEEMon Apr 07 1997 10:119
	Ran a line to the end of the conditioner pipe to supply slurry
	to the conditioner.

	Ran an N2 line from the fluids cabinet to the end of the conditioner, 
	waiting for parts to connect it to the main N2 line.


					
41.8Water in solenoidsFABSIX::R_GEEMon Apr 07 1997 10:175
	Tee'ed into the main CDA line and connected the DI water in, 
	RAW water in and chilled water in solenoids. This will allow
	the liquid to circulate even if the tool is powered off.

					
41.9GFI moduleFABSIX::R_GEEMon Apr 07 1997 10:246
	The tool wouldn't power up. Found that a door jumper had shorted
	out and blow the GFI module. We removed the jumpers and Speedfam 
	replaced the GFI module.

					
					
41.10#3 wafer lose sensorFABSIX::R_GEEMon Apr 07 1997 13:444
	Couldn't calibrate #3 wafer lose sensor, Speedfam replaced and
	calibrated. All set.
					
					
41.11installation of toolSUBPAC::CMPTue Apr 08 1997 12:155
    The installation is still continuing with a couple of minor problems,
    such as, a GFIC that was replaced, and a side door on the autoframe
    that was replaced due to warping.
    Checks and adjustments have been done, and we are now ready for the
    marathon.
41.12install continuesSUBPAC::CMPWed Apr 09 1997 20:385
    Installation continued today, finished running wafers from yesterday
    and replaced the 6 valves that were back flowing. Had some trouble with
    the robot mapping and corrected by adjusting and recalibrating. The
    testing will have to be restarted and we will continue tomorrow
    morning.
41.13Polish tub rinse valveFABSIX::R_GEEThu Apr 10 1997 19:092
	Connected the air line that opens 9AV38 (polish tub rinse)
	to the main CDA. 
41.14Mechanical acceptances stoppedFABSIX::R_GEEThu Apr 10 1997 20:4712
	On the second to last run of the 500 wafer mechanical acceptance
	marathon we lost a wafer on the pad from head #5 (believe it was at
	touchdown). Removed the wafers in queue using manual mode. Ran 25 
	more wafers, on the third run the system errored for no wafer on 
	carrier #1 (during load process). Checked carriers #1 & #5 cup to 
	load cup alignments and found them both off. Rebooted the too and 
	checked them again, they're still off. Field service has been notified
	and will be in in the morning.

	Note: We had to tighten the outside carrier screws at 450 wafers
	      most of them were falling out.
41.15completed marathonSUBPAC::CMPFri Apr 11 1997 20:473
    Well the marathon has been relegated to the history books. It looks
    like everything ran well and completed smoothly. The tool is sitting in
    wet mode for Mondays work.
41.16MARATON COMPLETED YESTERDAYFABSIX::B_WESTPHALSat Apr 12 1997 20:3191
pad#	runs	process		events
0	 50	DI only		system power down, GFI burnt. (replace next day)

	250	DI only		no issues
	 40	w monitors	failure: 6 block slurry manifold leaking by.
				replace slurry valve manifold
	 50    	DI only		NO ISSUES
	 40	DI only		assist: mapper  (fix + resume)
	 10	10 W		rate = ~2700, unif = ~4.5% (45,45)
~460	 50   	DI only		failure: mapper  (permenant sw fix + restart)
				pad is plistering at bubbles

0	 50	DI ONLY		assist: false wafer loss (calibrated s-5)
	 50    	DI only		NO ISSUES
	 25	DI only		NO ISSUES 
	replaced primary pad
	 40	DI only		NO ISSUES
	  5	W DUMMIES	NO ISSUES
50	  5	W MONITORS	NO ISSUES rate ~2800, unif = ~4.5% (45,45)
	 50	DI only		NO ISSUES
	 40	DI only		NO ISSUES
	  5	W DUMMIES	NO ISSUES (increase pre-wet to 15s from 5)
150	  5	W MONITORS	NO ISSUES rate 2910, unif = 2.7%  (45,45)
	 50	DI only		NO ISSUES
	 40	DI only		NO ISSUES
	  5	W DUMMIES	NO ISSUES
250	  5	W MONITORS	NO ISSUES rate 3213,unif = 2.9% (t=35,c=45)
	 50	DI only		NO ISSUES
	 40	DI only		NO ISSUES
	  5	W DUMMIES	NO ISSUES
350	  5	W MONITORS	NO ISSUES rate 3330,unif = 5.6% (t=35,c=45)
	 50	DI only		NO ISSUES
	 40	DI only		NO ISSUES
	  5	W DUMMIES	NO ISSUES
450	  5	W MONITORS	NO ISSUES rate 3432,unif = 6.19% (t=35,c=45)
	 35	DI only		Wafer crash (slide out at TD from head-5)
				Alligbnents were out.
				Restart and system errored for wafer out not in
			   	carrier 1, vacuum low.

  Allignments recalibrated. Loose bolt on index table motor tightened. Index
table voltage offset change to .62v frm 0. Restart test and system errored
again for low vacuum carrier-1. Vacuum filter was found clogged. The root cause
is inadequate vacuum tank blow down. The system only blows down the vacuum tank
when it is started from and IDLE position, when it is run in continouse 
(cassetetes placed in the system one after the other) it does NOT dump the tank.
This is how we ran most of the marathon and beleive to have caused water to 
biuld up in the tabk and vacuum system. Filter changed amnd 500 wafer test 
restarted.


 New pad, new DF-200 carriers

	 50	DI only		NO ISSUES
	 50	DI only		NO ISSUES
	 15	DI only		NO ISSUES
	  5	W DUMMIES	NO ISSUES 
125	  5	W MONITORS	assist: robot missed w #25 cass-A
	 15	DI only		NO ISSUES
	  5	W DUMMIES	NO ISSUES 
150	  5	W monitors	rate , unif = %  (35,45, met 202)
	 25	DI only		No issues
	 50	DI only		No issues
	 15	DI ONLY		No issues
	  5	w dummies	NO issues
250	  5	W monitor	Assist: Robot mised wafer top of cassette A
				Restarted and same error. Robot retaught,
				Marathon restarted.
      restart = 0
	 50	DI only		No issues
	 15	DI ONLY		No issues
	  5	w dummies	NO issues
325	  5	W monitor	rate =, unif =
	 25	DI only		No issues
	 25	DI only		No issues
	 25	DI only		No issues
	 50	DI only		No issues
	carrier screws loose, tightened same.
	 15	DI ONLY		No issues
	  5	w dummies	NO issues
450	  5	W monitor	rate =, unif =
	 25	DI ONLY		No issues 
	 50	DI only		No issues
	 50	DI only		No issues
	 50	DI only		No issues
675	 50	DI only		No issues
	____
	500     Maraton completed


41.17TOOL CLEANED/N2 GUN/FILTER HOUSINGS NOT INFABSIX::B_WESTPHALSat Apr 12 1997 20:338
CMP.D1- The process area was scubbed down as requested by engineering.  The 
	tungston stains came off fairly easy with only tex wipes & IPA.
	An N2 gun was hooked up.  We went to Packaging Plus to pick up the
	vacuum filter housings but FEDEX never got the parts here.  We checked 
	at the HLO1 security desk but it wasn't there either.


41.18regulator/shutoff for cond arm now onlineSUBPAC::LANDRYSun Apr 13 1997 12:566
    The shut-off valve and pressure regulator for the condition arm N2
    setup has been installed, and is quite functional.  It's now ready
    for Engineering evaluation.
    
                                           "A" shift
      
41.19Primary polish tube rinse / DI leakFABSIX::R_GEEMon Apr 14 1997 17:367
	Moved the 1/8" air line from 9SV13 to the main CDA line so the
	primary polish tube rinse stays open for continuous rinsing.

	Repaired a DI water leak coming from the main line for table 
	rinse.  
					
					
41.20pad conditioner rinse stationFABSIX::R_GEETue Apr 15 1997 10:134
	Modified the pad conditioner rinse station and conditioner
	fittings so it submerges into the rinse station properly.
					
					
41.21Mega System for Oxide slurryFABSIX::R_GEEThu Apr 17 1997 12:435
	The mega system is on-line for oxide slurry. Put a pressure
	gauge in-line with pump #6, we have flow but no pressure
	Ashland's has been called and is working the issue.
					
					
41.22Vacuum pump filterFABSIX::R_GEEThu Apr 17 1997 12:453
	Replaced the vacuum pump filter with the clean housing type,
	same as all the "B" tools.					
					
41.23ChillerFABSIX::R_GEEMon Apr 21 1997 18:518
	Couldn't control the remote chiller temp. Found the Access cable
	between the tool and the chiller was wired wrong. Removed the
	wires from pins #8 & #13 and soldered them onto pins #6 & #7.

	In IO module rack #1 slot #7 we moved wire #1178 from pin #1 
	to pin #3, Per TSB A7012A-A. this is the output to the chiller.

	Set the chiller temp. to 15c 
41.24Screen locked upFABSIX::R_GEEMon Apr 21 1997 19:177
	After the chiller work was completed we put the tool into
	Wet Mode and left the room. 20 minutes later returned to the 
	room and found the tools screen frozen on the Operations
	screen, with 4 thick black vertical lines in it. Re-booted 
	the tool, it seems to be o.k. now.

					A shift 
41.25Screen locked upFABSIX::R_GEETue Apr 22 1997 19:524
	Came in this morning, the tool was in wet mode but the
	screen was locked up again, Kevin re-booted the tool. 

					A shift & SF
41.26chiller wouldn't cool to set pointFABSIX::R_GEETue Apr 22 1997 20:3012
	The chiller wouldn't cool to 15c, it would go down to 22c and 
	that was it.

	Checked the incoming PCWS, the flow was 0 gpm at 70 lbs of 
	pressure. Found the incoming PCWS valve inside the chiller
	was closed, this was tripping the compressor off. Loosened 
	the tention screw so the spring would allow the valve to open 
	and reset the compressor, all set.

	Checked the actual temp. of the fluid inside the reservoir and 
	it matches the display. 
					A shift & SF
41.27Screen locked up / slurry to barrel lines removedFABSIX::R_GEEWed Apr 23 1997 20:0718
	When Earl tried to start the tool today he mapped the cassettes
	and went to the Operation screen. When he pressed start, the button
	turned green but didn't do anything, after about 3 minutes he
	then pressed Pause, it also turned green (start & pause both green).

	We tried to abort but it wouldn't respond. It would only allow us
	to backout to the main menu and that was it. Everytime we tried to 
	move into another function menu it would say (not allowed unless
	the system is idle). Had to re-boot the tool, all set for now.
	Speedfam has a TSB and hardware that should repair the lockup 
	problems.

	Cleaned out the oxide slurry lines and removed them from the 
	barrel and the tool. Before the tool can be run the lines need
	to be reconnected to slurry pump lines #4 & #5 then the lines
	put back into the slurry barrel. 

						A shift
41.28CARRIER SCREWSYIELD::TDYERFri Apr 25 1997 17:5228
Carrier screw and ring guide update:

 During W-CMP processing the carrier screws are loosening and the ring guides 
are cracking. We believe this is caused by vibration shock waves transmitting
through the polish table and into the carrier. Unlike the IC1000/Suba-4, the
PAN-W pad is very hard, very thin and offers no dampening. Carrier construction
materials will be optimized to alleviate this problem. In the interim, process 
Engineering will tighten the carrier screws every 50 wafers. We have built 
several test carriers for evaluation. They will be installed on Monday AM and
used during Process DOEs. The carriers are built as follows:

	Backing plate torque = 15"/lbs
	Ring guide initial torque = 8"/lbs
	exposures = .005 - .006"

	carrier-1	standard lockwashers
	carrier-2	standard lock w. + locktight on washers
	carrier-3	split lock washer
	carrier-4	split lock w. + locktight on washers
	carrier-5	split lock washer on top of plastic washer

  The PPS carrier ring would not come in spec, all ring guides are Delrin.
 We will be testing more washer and ring schemes plus experimenting with
 compressible shims.

 Tim/Brad/Sammy

41.29#2 load cup / Slurry pumps cal'edFABSIX::R_GEEMon Apr 28 1997 19:3615
	- Two wafers slid out from under carrier #2, crashed twice.

		Found that carrier #2 unload cup was in the #2 load
		cup position.
	
	- Checked slurry flows for pumps #1 thru #3, all out.
          Changed the Eng./Scale factor to correct.
 
			   pre      post
		pump #1    150      120
		pump #2    150      127
		pump #3    150      110


					A shift
41.302% Citric to scrub brushes / Robot & DI waterFABSIX::R_GEEMon Apr 28 1997 19:5428
	* Process Eng. requested a way to pump 2% Citric acid into the 
	  scrub station brushes.

	    Put a "tee" in-line after the DI water solenoid feeding the 
	    scrub station brushed. And installed a pump under the elevators.

	    To operate the pump:  

		- Remove the air line for the scrubber brush DI solenoid
		  under elevator #1.

		- Remove the cap from the "tee" and connect the hose for 	
		  the pump. 


	========================================================

	* While connecting the above we sprung a DI water leak.

	  Had to replace the Automation frame #46 fuse, (dual outlet). 
	  Dry out the robot controller, hand pendent & cables.

	  Tried to power the tool up, the robot wouldn't home, found
	  the cables had fallen off the robot. The cables between the
	  robot body and the controller are just pushed on, not screwed.
	  These cable ends are broken and need to be replaced. 

					A shift & Tim
41.31Modified Carriers 3 & 4 Sray nosslesFABSIX::R_GEEMon Apr 28 1997 19:585
	Modified the carrier spray for carriers #3 & #4 so there is
	an additional spray nossle pointed down onto the carriers.

	Will do the rest tomorrow.
					A shift 
41.32Slurry pumps #4 & 5 cal'edFABSIX::R_GEETue Apr 29 1997 18:398
	Calibrated oxide slurry pumps #4 & #5, they were both low.
	We adjusted the Gain pods on the motor controlers for this
	Adjustment.

					A shift & Eng.



41.33Enhanced carrier spray has been modifiedFABSIX::R_GEETue Apr 29 1997 18:4911
 	Completed the installation of 5 additional carrier spray nozzles 
	on primary table to remove slurry from top of carriers. These are 
	activated by enhanced spray. Please be carefull when working around
	the primary polish table, if these are move you will need to 
	re-position them.

					A  shift
  
		


41.34Scrubber brushes changedFABSIX::R_GEEWed Apr 30 1997 12:238
	Changed the scrub station scrub brushed due to 
	high particles.
	

  
		


41.35Tool locked upFABSIX::R_GEEWed Apr 30 1997 17:1610
	The tool locked up in the operations screen, both start and 
	pause were lit, had to re-boot the tool. Found out later
	in the day, when it locked up again, if you back out and re-seize
	control then start over you can recover. There is a TSB
	and hardware on the cabinet in the room that Speedfam needs 
	to install that should take care of this problem.
  
		


41.36Carrier retainer ring screw set-upFABSIX::R_GEEWed Apr 30 1997 17:3814
	Yesterday, all the carriers retainer ring screws, except for 
	carrier #2, loosened after only 15 wafers. Carrier #2 was built
	with standard lock washers and loctite on washers. Re-built all 
	5 carriers this morning using the above setup at 12 lbs. Ran 
	70 wafers & checked the screws after each cassette, no loose screws.
	
		Looks like this, "Standard lock washers with loctite on the 
		washers & screws", will keep the retainer ring screws 
		from backing out. 
  
		


41.37Slurry lines and hingesSUBPAC::BJUBINVILLECMP Equipment EngineeringFri May 02 1997 06:548
    
           Replaced the slurry lines on Slurry #5 and #6.
        Per Tim we didn't check flow...
    
           Replaced top broken hinge on the front lower
        left door.
    
                                        BJ
41.38elv-1, w-loss-1YIELD::TDYERMon May 05 1997 02:089
    
    Head-1 wafer loss sensor detecting false wafers, adjusted same.
    Elevator-1 would not home. The level sensor float became wedge in
    the elevator base, re-installed same. Also noted that the enhanced-
    enhanced DI spray can not be turned on with the carriers down, it
    will get the multi-head underside wet.
    
    Tim + B shift